N857SW

Substantial
Minor

CIRRUS DESIGN CORP SR22TS/N: 0816

Accident Details

Date
Tuesday, November 3, 2015
NTSB Number
CEN16LA026
Location
Fayetteville, AR
Event ID
20151103X33454
Coordinates
36.056667, -94.174446
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
2
Uninjured
1
Total Aboard
3

Probable Cause and Findings

The fatigue failure of the oil cooler cross fitting, which resulted in engine oil starvation and a total loss of engine power.

Aircraft Information

Registration
N857SW
Make
CIRRUS DESIGN CORP
Serial Number
0816
Engine Type
Reciprocating
Year Built
2014
Model / ICAO
SR22TSR22
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
WG AVIATION LLC
Address
24 PINNACLE DR
Status
Deregistered
City
ROGERS
State / Zip Code
AR 72758
Country
United States

Analysis

HISTORY OF FLIGHTOn November 3, 2015, at 0950 central standard time, a Cirrus SR22T airplane, N857SW, experienced a total loss of engine power, descended under the canopy of the Cirrus Airframe Parachute System (CAPS) and landed on a road in Fayetteville, Arkansas. The private rated pilot, pilot rated passenger and one person on the ground received minor injuries. The passenger in the right rear seat was uninjured. The airplane sustained substantial damage. The airplane was registered to WG Aviation LLC, Rogers, Arkansas, and operated by a private individual under the provisions of 14 Code of Federal Regulations Part 91 as a personal flight. Visual meteorological conditions prevailed at the time of the accident and an instrument flight rules (IFR) flight plan was filed. The flight departed from Bentonville Municipal Airport (VBT), Bentonville, Arkansas, at 0934 and was en route to Waco Regional Airport (ACT), Waco, Texas.

According to the pilot, after departure from VBT he leveled off around 10,000 ft mean sea level (msl) and was above a cloud layer. The pilot noticed that the crew alerting system (CAS) flashed an amber caution light for oil pressure and the engine was still producing normal power. The pilot notified air traffic control (ATC) of the oil pressure issue and received vectors to the nearest airport, Drake Field Airport (FYV), Fayetteville, Arkansas. The pilot descended and maneuvered toward FYV as the CAS illuminated a red warning light for oil pressure, which had dropped below 10 psi. The engine was producing inconsistent power as the airplane descended to 3,300 ft msl. The pilot notified ATC that he could not maintain altitude and ATC declared an emergency on his behalf. About 3 miles from FYV the airplane was still above the cloud layer and he could not see the airport or runway. The airplane slowed to 80 knots around 1,000 ft above ground level (agl) and the stall warning horn sounded. He deployed the CAPS and the airplane descended to the ground under the canopy. The landing was very firm and the seatbelt airbags deployed. PERSONNEL INFORMATIONThe pilot, age 56, held a private pilot certificate with ratings for airplane single engine land and instrument airplane. On February 26, 2014, the pilot was issued a third class medical certificate with no limitations listed.

The pilot rated passenger, age 47, held an airline transport pilot certificate. He also held a flight instructor certificate for single engine airplane and instrument airplane. On July 20, 2015, he was issued a first class medical certificate with one limitation: must wear corrective lenses. AIRCRAFT INFORMATIONThe Cirrus SR22T four seat, low wing, fixed tricycle landing gear airplane, serial number 0816, was manufactured in 2014. The airplane was powered by a 315-horsepower, turbocharged, Continental Motors TSIO-550-K engine, which drove a 3-bladed, composite, constant speed Hartzell propeller.

A review of the airplane logbooks revealed that a 50 hour engine inspection was completed on September 30, 2015, at a total time of 232.4 hours and Hobbs meter time of 288.9 hours.

A maintenance work order, opened September 24, 2015, and closed October 7, 2015, revealed under discrepancy 6 to comply with Continental Motors Critical Service Bulletin CSB15-2 – Oil Cooler Cross Fitting Replacement. The maintenance was deferred to a later date because the "owner was out of time to wait and requested" to complete the CSB during the next maintenance service. The work order also noted that the CSB was deferred due to the engine manufacturer being out of stock of oil cooler cross fittings. According to the maintenance facility inventory report, four oil cooler cross fittings were received from the engine manufacturer on September 29, 2015, immediately after they were back in stock. The pilot had already decided to defer this CSB, therefore it was not completed. METEOROLOGICAL INFORMATIONAt 0953, the weather observation at FYV recorded wind from 190 at 9 knots, gusting to 17 knots, 10 miles visibility, clear sky, temperature 61° F, dew point 57° F, and altimeter setting 30.11 inches of mercury. AIRPORT INFORMATIONThe Cirrus SR22T four seat, low wing, fixed tricycle landing gear airplane, serial number 0816, was manufactured in 2014. The airplane was powered by a 315-horsepower, turbocharged, Continental Motors TSIO-550-K engine, which drove a 3-bladed, composite, constant speed Hartzell propeller.

A review of the airplane logbooks revealed that a 50 hour engine inspection was completed on September 30, 2015, at a total time of 232.4 hours and Hobbs meter time of 288.9 hours.

A maintenance work order, opened September 24, 2015, and closed October 7, 2015, revealed under discrepancy 6 to comply with Continental Motors Critical Service Bulletin CSB15-2 – Oil Cooler Cross Fitting Replacement. The maintenance was deferred to a later date because the "owner was out of time to wait and requested" to complete the CSB during the next maintenance service. The work order also noted that the CSB was deferred due to the engine manufacturer being out of stock of oil cooler cross fittings. According to the maintenance facility inventory report, four oil cooler cross fittings were received from the engine manufacturer on September 29, 2015, immediately after they were back in stock. The pilot had already decided to defer this CSB, therefore it was not completed. WRECKAGE AND IMPACT INFORMATIONThe airplane landed on the east bound side of a four lane road in Fayetteville, Arkansas. The airplane impacted a moving vehicle, then a curb, and came to rest on the sidewalk with the nose facing east. The left landing gear had partially collapsed outward, the right landing gear was separated, and the nose landing gear had collapsed and separated. The left wing sustained leading edge damage near the wing tip. The right wing sustained damage to the leading edge near the wing root. The bottom of the fuselage was damaged. A black oily residue was observed from the bottom of the fuselage to the bottom tip of the rudder. The parachute was found on the ground behind the airplane.

A postaccident examination was conducted on November 4, 2015. During the examination there was no evidence of a breach in the crankcase or the oil sump; however, the nipple fitting that connected to the oil cooler cross fitting was separated and oil residue was observed in the engine compartment. The top spark plugs were removed and found to be in "normal condition" when compared to a Champion Aviation Check-A-Plug AV-27 chart. However, each of the top spark plugs exhibited a dark, sooty coloration indicative of a rich fuel air mixture. Each of the six cylinders were examined with a lighted borescope. The intake and exhaust valves were intact with normal coloration and combustion signatures. The damaged propeller was manually rotated revealing that the internal engine components were "tight" and not easily rotated. The oil dipstick was removed and the engine oil level appeared to be 1 to 2 quarts. All fuel system components remained intact and attached to the engine. The magnetos remained intact and in place with no apparent impact damage. All other engine accessories were intact and unremarkable.

Engine Examination and Disassembly

The engine was disassembled at the engine manufacturer's facility on November 23, 2015, under the supervision of the NTSB. The examination revealed that the nipple fitting that connected to the oil cooler cross fitting had fractured. The cross fitting had several tool marks on the flat sides of the part. The engine exhibited mechanical damage signatures on all rod and main bearing journals. The Nos. 1 and 3 rods had released from the crankshaft and internal damage to the interior of the crankcase was noted. The oil pump was examined and there was no indication of hard particle passage noted. The oil sump contained metal fragments of the rod bearings from the released connecting rods. The remainder of the engine exhibited normal operating signatures, with the exception of the mechanical and thermal damage. ADDITIONAL INFORMATIONRecorded Flight Data – Cirrus Recoverable Data Module

The airplane's recoverable data module (RDM) was removed and sent to the NTSB Vehicle Recorders Laboratory for download. The data revealed that the airplane departed and climbed at a constant speed with the oil pressure indicating about 50 psi. At 0943:30, as the airplane was climbing through 9,500 ft msl, the oil pressure began to decrease. The airplane reached a peak altitude of 9,830 ft msl. At 0944 the oil pressure had decreased to 36 psi and the airplane made a left turn and started to descend. The airplane descended for about 7 minutes as the oil pressure decreased about 0.5 psi per second until it reached about 3 psi. Engine RPM decreased to 0 as oil pressure decreased below 1 psi at 0950:30.

Continental Motors Critical Service Bulletin CSB15-2 – Oil Cooler Cross Fitting Replacement

The CSB15-2 was originally published on July 2, 2015, and the purpose was to replace the old oil cooler cross fitting with a new enhanced cross fitting within the next 25 hours of engine operation or the next scheduled inspection or engine servicing, whichever occurred first." The bulletin noted "compliance necessary to maintain safety" and further stated "Continental Motors, Inc. (CMI) is aware of some occurrences in which the there was a loss of engine oil due to a fractured nipple fitting that connects the cross fitting to the pipe bushing at the oil cooler. Design improvements consolidate the oil cooler cross fitting stack-up into a single part, which significantly increases the strength and provides a simplified installation procedure for installing the oil cooler cross fitting found on specified TSIO-550 and TSIOF-550 engines."

CSB15-2A – The bulletin was revised on October 30, 2015, with updated warranty information and updated illustrated parts catalog instructions.

CSB15-2B – As a res...

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN16LA026