N688KA

Substantial
Minor

SWEENEY TIMOTHY J RANS S6-ESS/N: 05081884-ES

Summary

On November 13, 2015, a Sweeney Timothy J RANS S6-ES (N688KA) was involved in an accident near Winter Haven, FL. The accident resulted in 1 minor injury. The aircraft sustained substantial damage.

The National Transportation Safety Board determined the probable cause of this accident to be: The pilot's improper landing flare, which resulted in a nose gear collapse and nose over.

The pilot reported that during an intentional landing on the grass parallel to an asphalt runway, he touched down fast and bounced "slightly." He then became distracted when another pilot reported over the radio that a coyote was crossing the runway. Subsequently, he "let the nose wheel down too early and too quickly." The nose gear collapsed and the airplane nosed over. The vertical stabilizer was substantially damaged.

The pilot reported that there were no mechanical malfunctions or failures with the airplane that would have precluded normal operation.

This accident is documented in NTSB report GAA16CA053. AviatorDB cross-references NTSB investigation data with FAA registry records to provide comprehensive safety information for aircraft N688KA.

Accident Details

Date
Friday, November 13, 2015
NTSB Number
GAA16CA053
Location
Winter Haven, FL
Event ID
20151119X04728
Coordinates
28.062778, -81.751945
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
1
Uninjured
0
Total Aboard
1

Probable Cause and Findings

The pilot's improper landing flare, which resulted in a nose gear collapse and nose over.

Aircraft Information

Registration
Make
SWEENEY TIMOTHY J
Serial Number
05081884-ES
Year Built
2009
Model / ICAO
RANS S6-ES

Registered Owner (Historical)

Name
SALE REPORTED
Address
8057 LICK FORK RD
Status
Deregistered
City
WITTS SPRINGS
State / Zip Code
AR 72686-1377
Country
United States

Analysis

The pilot reported that during an intentional landing on the grass parallel to an asphalt runway, he touched down fast and bounced "slightly." He then became distracted when another pilot reported over the radio that a coyote was crossing the runway. Subsequently, he "let the nose wheel down too early and too quickly." The nose gear collapsed and the airplane nosed over. The vertical stabilizer was substantially damaged.

The pilot reported that there were no mechanical malfunctions or failures with the airplane that would have precluded normal operation.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# GAA16CA053