N72MTWAYLAND JOHN H AVID MARK IV2016-01-09 NTSB Accident Report

Substantial
Serious

WAYLAND JOHN H AVID MARK IVS/N: 1431D

Summary

On January 09, 2016, a Wayland John H AVID MARK IV (N72MT) was involved in an accident near Minneola, FL. The accident resulted in 1 serious injury. The aircraft sustained substantial damage.

The National Transportation Safety Board determined the probable cause of this accident to be: A total loss of engine power for reasons that could not be determined because postaccident examination revealed no anomalies that would have precluded normal operation. Contributing to the accident was the pilot's exceedance of the airplane’s critical angle of attack during the crosswind turn, which resulted in an aerodynamic stall/spin.

On January 9, 2016, about 1600 eastern standard time, an experimental amateur-built Avid Mark IV, N72MT, was substantially damaged following a forced landing after takeoff from Florida Flying Gators Ultralight Flightpark (3FD4), Minneola, Florida. The sport pilot was seriously injured. The airplane was privately owned and operated under the provisions of 14 Code of Federal Regulations Part 91 as a personal flight. Day, visual meteorological conditions prevailed, and no flight plan was filed. The local flight was originating at the time of the accident.The pilot reported that, after takeoff, he turned onto the crosswind leg of the traffic pattern. He performed a steep turn after takeoff to avoid horses off the end of the runway.

This accident is documented in NTSB report ERA16LA086. AviatorDB cross-references NTSB investigation data with FAA registry records to provide comprehensive safety information for aircraft N72MT.

Accident Details

Date
Saturday, January 9, 2016
NTSB Number
ERA16LA086
Location
Minneola, FL
Event ID
20160111X11353
Coordinates
28.627777, -81.802780
Aircraft Damage
Substantial
Highest Injury
Serious
Fatalities
0
Serious Injuries
1
Minor Injuries
0
Uninjured
0
Total Aboard
1

Probable Cause and Findings

A total loss of engine power for reasons that could not be determined because postaccident examination revealed no anomalies that would have precluded normal operation. Contributing to the accident was the pilot's exceedance of the airplane’s critical angle of attack during the crosswind turn, which resulted in an aerodynamic stall/spin.

Aircraft Information

Registration
Make
WAYLAND JOHN H
Serial Number
1431D
Year Built
2000
Model / ICAO
AVID MARK IV

Registered Owner (Historical)

Name
SALZMANN ROBERT E
Address
2039 COLLIER DR
Status
Deregistered
City
FERN PARK
State / Zip Code
FL 32730-3103
Country
United States

Analysis

On January 9, 2016, about 1600 eastern standard time, an experimental amateur-built Avid Mark IV, N72MT, was substantially damaged following a forced landing after takeoff from Florida Flying Gators Ultralight Flightpark (3FD4), Minneola, Florida. The sport pilot was seriously injured. The airplane was privately owned and operated under the provisions of 14 Code of Federal Regulations Part 91 as a personal flight. Day, visual meteorological conditions prevailed, and no flight plan was filed. The local flight was originating at the time of the accident.The pilot reported that, after takeoff, he turned onto the crosswind leg of the traffic pattern. He performed a steep turn after takeoff to avoid horses off the end of the runway. He then noticed the smell of "burning wires" and "may have seen a wisp of smoke." At 300 feet above the ground, and while still climbing, the engine "sputtered, then died." He made a radio call that he was returning to the runway. The left wing then stalled and the airplane rolled inverted and entered a downward spiral. The airplane collided with two trees during the descent before colliding with the terrain. The airplane came to rest in a grassy area, inverted.

Inspectors with the Federal Aviation Administration (FAA) responded to the accident site and examined the wreckage. They observed structural damage to fuselage, empennage, and both wings. An FAA airworthiness inspector examined the engine and found no evidence of a mechanical failure or malfunction. There were no arcing or burn signatures on the engine's electrical wiring or connectors. A postaccident test run of the engine could not be performed due to impact damage.

The pilot received his sport pilot certificate on September 2, 2015, after taking a two-week training course. He reported 120 hours of total flight time, including 100 hours as pilot-in-command. He also reported 65 hours in the accident airplane make and model, all as pilot-in-command. He stated that, after the accident, he took additional lessons with his original flight instructor to practice emergency procedures, stalls, and stall recovery.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA16LA086