N9262M

Substantial
Minor

MOONEY M20CS/N: 3456

Accident Details

Date
Friday, March 18, 2016
NTSB Number
CEN16LA129
Location
Wichita, KS
Event ID
20160322X70716
Coordinates
37.726665, -97.228614
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
2
Uninjured
0
Total Aboard
2

Probable Cause and Findings

The total loss of engine power due to fuel starvation, which resulted from the pilot's improper fuel management.

Aircraft Information

Registration
N9262M
Make
MOONEY
Serial Number
3456
Engine Type
Reciprocating
Year Built
1966
Model / ICAO
M20CM20P
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
SABRIS CORP
Address
6716 BAINBRIDGE RD
Status
Deregistered
City
WICHITA
State / Zip Code
KS 67226-1049
Country
United States

Analysis

On March 18, 2016, about 1525 central daylight time, a Mooney M20C, N9262M, lost engine power while on approach to the Col. James Jabara Airport (AAO), Wichita, Kansas, and subsequently collided with terrain. The pilot and his passenger received minor injuries. The airplane was substantially damaged. The airplane was registered to and operated by the Sabris Corporation, Wichita, Kansas, under the provisions of 14 Code of Federal Regulations Part 91 as a personal flight. Visual meteorological conditions prevailed at the time of the accident, and no flight plan had been filed. The flight originated from Dickson (M02), Tennessee, about 1130 was en route to AAO.

According to the pilot's statement, he had preflighted the airplane in M02 and noted that both fuel tanks were "filled to the rim." (According to the Mooney Aircraft Corporation, fuel capacity for the model M20C is 52 gallons, 26 gallons per wing tank). The flight to AAO was uneventful. Due to inbound IFR (instrument flight rules) traffic, the pilot extended the downwind leg for landing when the engine suddenly lost power. The pilot said he used the ALARMS (airspeed, landing site, air restart, radios, mayday, secure plane) checklist. The airplane was too far from the runway, so the pilot attempted to land on a golf course. He did not recall the forced landing and woke up in an ambulance en route to the hospital.

A Federal Aviation Administration inspector who examined the airplane reported finding "no discernible quantity of fuel in the left tank." The fuel selector was positioned on the left fuel tank, and the electric fuel pump was in the off position. When the airplane was placed in a level position, the inspector was not able to sump fuel from the left fuel tank, even with the electric fuel pump running, or from the fuel selector valve sump. Some fuel was noted in the right fuel tank. The inspector was able to sump fuel from the right fuel tank. The fuel level was about 2 to 3 inches in depth. There was no evidence of fuel spillage, and the fuel tanks did not appear to have been breached. There were no fuel stains on the ground or the smell of fuel around the airplane. No other anomalies or mechanical failures were noted.

Airplane damage consisted of a buckled lower fuselage from the engine cowling aft to the rear bulkhead. The firewall was bent. The right wing leading edge bore crush damage, and the main landing gear was pushed up through the wing. The flap was also bent.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN16LA129