N302CT

Destroyed
Minor

FLIGHT DESIGN GMBH CTSW HXBS/N: 07-06-06

Accident Details

Date
Wednesday, June 15, 2016
NTSB Number
CEN16LA221
Location
Sealy, TX
Event ID
20160616X23207
Coordinates
29.733333, -96.059165
Aircraft Damage
Destroyed
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
2
Uninjured
0
Total Aboard
2

Probable Cause and Findings

Failure of maintenance personnel to comply with the engine manufacturer’s mandatory service bulletin, which resulted in failure of the mechanical fuel pump diaphragm and a subsequent total loss of engine power.

Aircraft Information

Registration
N302CT
Make
FLIGHT DESIGN GMBH
Serial Number
07-06-06
Engine Type
Reciprocating
Year Built
2007
Model / ICAO
CTSW HXBFDCT
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
MAYIONOS SPIRO
Address
4044 S BRAESWOOD BLVD
Status
Deregistered
City
HOUSTON
State / Zip Code
TX 77025-3304
Country
United States

Analysis

On June 15, 2016, about 1430 central daylight time, a Flight Design GMBH CTSW HXB, N302CT, collided with trees during a forced landing at Gloster Aerodrome (1XA7), Houston, Texas. The student pilot and flight instructor both sustained minor injuries. The airplane was destroyed. The airplane was registered to and operated by the student pilot under the provisions of 14 Code of Federal Regulations Part 91 as an instructional flight. Visual meteorological conditions prevailed at the time of the accident, and no flight plan had been filed. The local flight had just originated.According to the flight instructor, the student pilot made the takeoff on runway 25. During the initial climb (about 500 feet AGL), the engine started running rough and lost all power. The instructor took control of the airplane and made a 180-degree turn back towards the airport. A forced landing to runway 07 was attempted but due to a strong tailwind, the airplane collided with trees to the right of the runway.

On October 20, under the auspices of a Federal Aviation Administration (FAA) inspector, the engine was examined at the facilities of South Mississippi Light Aircraft in Lucedale, Mississippi. A Rotax engine representative was also in attendance. Reportedly, the engine would not start on the first attempt. It was determined that the engine was not receiving fuel due to a leak in the fuel pump diaphragm. When an electric fuel pump on the engine test stand was turned on, fuel poured out of the fuel pump drain hole. Disassembly of the fuel pump confirmed that the rubber diaphragm had deteriorated and was leaking. When a serviceable fuel pump was installed, the engine operated normally and produced full power. No further anomalies were noted.

According to the engine logbook, Rotax Service Bulletin SB-912-053-UL (Replacement of fuel pump for Rotax Engine Type 912), dated April 13, 2007, had been complied with on May 24, 2006 (see page 5 of manual). However, Rotax Service Bulletin SB-912-063-UL (Replacement for fuel pumps for Rotax Engine Type 912), dated August 21, 2013, had not been performed. The fuel pump that was installed on the engine (part number 892 542, serial number 07.002314) was manufactured in 2009 and was affected by this service bulletin but it was not listed in the log book. The fuel pump was also affected by Bombardier's Recreational Products Maintenance Manual, requiring a mandatory replacement time of 5 years. Following the recommended replacement date of May 24, 2012, annual inspections of the engine were conducted on November 12, 2012, May 2, 2014, and June 6, 2016. A conditional engine examination was performed on June 13, 2015.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN16LA221