N30923

Destroyed
Minor

CESSNA 177S/N: 17701548

Accident Details

Date
Monday, August 8, 2016
NTSB Number
ERA16LA286
Location
McDonough, NY
Event ID
20160808X03845
Coordinates
42.443054, -75.803886
Aircraft Damage
Destroyed
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
4
Uninjured
0
Total Aboard
4

Probable Cause and Findings

The pilot’s improper recovery from a slow flight configuration at low altitude, which resulted in an exceedance of the airplane’s critical angle of attack and an aerodynamic stall. Contributing to the accident was the pilot’s decision to operate at low altitude.

Aircraft Information

Registration
N30923
Make
CESSNA
Serial Number
17701548
Engine Type
Reciprocating
Year Built
1970
Model / ICAO
177C177
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
MEI-CHU CORP
Address
C/O JAO-SHIANG LUO
4532 158TH ST
Status
Deregistered
City
FLUSHING
State / Zip Code
NY 11358-3144
Country
United States

Analysis

On August 8, 2016, about 1535 eastern daylight time, a Cessna 177B, N30923, was destroyed when it impacted trees and terrain while maneuvering near McDonough, New York. The private pilot and three passengers sustained minor injuries. Visual meteorological conditions prevailed and no flight plan was filed for the personal flight, which originated from Sidney Airport (N23), Sidney, New York and was destined for Brookhaven Airport (HWV), Shirley, New York. The airplane was operated under the provisions of 14 Code of Federal Regulations Part 91.During an interview, the pilot stated that prior to the accident flight, he filled the airplane's fuel tanks, for a total fuel load of 50 gallons. The purpose of the flight was to fly back to HWV, where the airplane was based, and give the three passengers an opportunity to view and photograph a local landmark on-the-way. After making two passes over the landmark, the passengers asked the pilot to flyover again, but at a slower speed. The pilot then fully deployed the flaps in preparation for the next flyover. During the flyover, the pilot noted that the airplane was slow, and had descended to a height near the tops of the trees. He added full power and fully retracted the flaps. The airplane did not appear to be climbing, and in "a wink of an eye the nose dropped." The pilot was then looking straight down at the ground. The pilot's next recollection was that the airplane was on the ground. He and his passengers subsequently egressed before the airplane was consumed by a postimpact fire.

During separate statements to a Federal Aviation Administration (FAA) inspector, first responders and an NTSB investigator, the pilot did not report any mechanical functions during the accident flight. In a subsequent written statement he reported that the engine experienced a total power loss prior to the impact.

One of the passengers reported that he and the other two passengers were taking pictures of the landmark when he noticed the airplane descending and then hitting a tree. He did not remember hearing anything strange before the accident. Another witness that was standing on the north side of the landmark, saw the airplane fly overhead three times. During the third flyover, the airplane was flying north very low near the tree tops. He then heard the breaking of branches and a loud bang. He stated he ask someone to call 911 while he tried to help the passengers out of the airplane. Shortly after they all were out of the airplane, it erupted in flames.

Examination of the wreckage by an FAA inspector revealed that the airplane was destroyed by fire. The engine was intact, but exhibited extensive thermal damage. All other components were unrecognizable.

The weather conditions reported at Greater Binghamton Airport, Binghamton, New York, located 16 nautical miles south of the accident site, at 1553, were clear sky, wind calm, and visibility 10 statute miles.

The pilot held a private certificate with a rating for airplane single-engine land. He also held a third-class medical certificate, issued on June 24, 2016. His last flight review was completed on June 27, 2015. At the time of the accident, the pilot reported 378 total hours of flight experience, with 100 hours in the same make and model as the accident airplane.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA16LA286