N526AM

Substantial
Fatal

MOONEY M20JS/N: 24-0916

Accident Details

Date
Sunday, September 25, 2016
NTSB Number
ERA16FA325
Location
Pittstown, NJ
Event ID
20160926X05905
Coordinates
40.559444, -74.990554
Aircraft Damage
Substantial
Highest Injury
Fatal
Fatalities
2
Serious Injuries
0
Minor Injuries
0
Uninjured
0
Total Aboard
2

Probable Cause and Findings

The pilot's improper landing touchdown attitude, which resulted in a propeller strike, and his inappropriate decision to abort the landing after the propeller had contacted the runway, which resulted in a loss of thrust and led to an aerodynamic stall during climb. Contributing to the accident was the pilot's lack of recent experience in the accident airplane make and model.

Aircraft Information

Registration
N526AM
Make
MOONEY
Serial Number
24-0916
Engine Type
Reciprocating
Year Built
1980
Model / ICAO
M20JM20P
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
SKINNER ILISSA
Address
106 SHARON RD STE B
Status
Deregistered
City
ROBBINSVILLE
State / Zip Code
NJ 08691-1309
Country
United States

Analysis

HISTORY OF FLIGHTOn September 25, 2016, about 1230 eastern daylight time, a Mooney M20J, N526AM, was substantially damaged when it impacted terrain during initial climb after a balked landing at Sky Manor Airport (N40), Pittstown, New Jersey. The private pilot and the passenger were fatally injured. The airplane was privately owned and operated under the provisions of Title 14 Code of Federal Regulations (CFR) Part 91. Visual meteorological conditions prevailed, and no flight plan was filed for the personal flight, which departed Pennridge Airport (CKZ), Perkasie, Pennsylvania, about 1200.

The pilot had rented the airplane at the Trenton-Robbinsville Airport (N87), Robbinsville, New Jersey. According to security camera video, he boarded the airplane and departed from N87 at 1121. The pilot flew to CKZ, where he picked up the passenger. The pilot then flew to N40 with the passenger.

Numerous witnesses at N40 reported that the pilot attempted twice to land on runway 25. During the first landing attempt, the airplane appeared to be fast on the final approach. During the touchdown, the airplane bounced. The pilot then aborted the landing, climbed out, and joined the traffic pattern.

Review of video recordings obtained from a security camera at N40 revealed that, during the second landing attempt, about 1229, the airplane touched down more than halfway down the length of the runway. The video recording also revealed that the airplane's wing flaps were extended, and a flag visible in the camera frame indicated that a variable right-quartering tailwind existed. Witnesses reported that, during the second landing attempt, the airplane was again fast on the approach, and it touched down first on the nose wheel, then on the main landing gear, bounced, and became airborne. The airplane bounced twice more, touched down about 400 to 500 ft before the end of the runway and remained on the runway surface. Witnesses heard the engine power increase as the airplane approached the end of the pavement, and the airplane began to climb.

The witnesses described that the airplane appeared to climb slowly as it passed over a field that was surrounded by trees at the end of the runway, and some witnesses reported that the engine did not seem to be producing full power. As the airplane approached the row of trees at the far end of the field, it appeared to climb steeply. The airplane cleared the row of trees and then abruptly banked steeply to the left, pitched nose down, and descended in a steep, nose-down attitude out of view behind the trees.

According to a witness who lived near the accident site, the airplane was flying very low and slow compared to many other airplanes that he had observed departing from N40. The airplane rose slightly, pivoted nose down, and then rapidly lost altitude as it went out of view behind a barn. According to another witness, he heard the airplane's engine running as it descended out of view. According to both witnesses, moments after losing sight of the airplane they heard the sound of impact. PERSONNEL INFORMATIONAccording to Federal Aviation Administration (FAA) records, the pilot held a private pilot certificate with an airplane single-engine land rating. His most recent FAA third-class medical certificate was issued on February 10, 2016. According to the pilot's logbook, he had accrued about 188 total hours of flight experience of which 36 hours were in the accident airplane make and model.

Review of the pilot's logbook revealed that his most recent flight before the accident flight was in a Piper PA-28-181, on January 14, 2016, about 8 months before the accident. Further review of the pilot's logbook revealed that the pilot's most recent flight in a Mooney M20J before the accident flight occurred on November 21, 2015, about 10 months before the accident. AIRCRAFT INFORMATIONThe airplane was a 4-place, complex, single-engine monoplane. The airframe had a tubular steel cabin frame covered with non-structural aluminum skins, a semi-monocoque tail cone, and a full cantilever laminar-flow wing. It was equipped with a retractable, electrically-operated, tricycle-type landing gear with rubber shock discs, a steerable nose wheel, and hydraulic disc brakes. It was powered by an air-cooled, fuel-injected, 200 horsepower, horizontally-opposed, four-cylinder, Lycoming engine driving a 2-blade, variable-pitch, constant-speed McCauley propeller.

According to FAA and airplane maintenance records, the airplane was manufactured in 1980. The airplane's most recent 100-hour inspection was completed on August 13, 2016. At the time of the inspection, the airplane had accrued about 4,690.3 total hours of operation, and the engine had accrued about 100 hours of operation since major overhaul. METEOROLOGICAL INFORMATIONAt 1253, the recorded weather at Somerset Airport (SMQ), Somerville, New Jersey, located 15 nautical miles east of the accident site, included wind 350° at 10 knots, visibility 10 miles, sky clear, temperature 21°C, dew point -1°C, and an altimeter setting of 30.17 inches of mercury. Calculation of the crosswind component using the recorded weather at SMQ indicated that about a 2-knot tailwind would have been present on runway 25 at N40 about the time of the accident. AIRPORT INFORMATIONThe airplane was a 4-place, complex, single-engine monoplane. The airframe had a tubular steel cabin frame covered with non-structural aluminum skins, a semi-monocoque tail cone, and a full cantilever laminar-flow wing. It was equipped with a retractable, electrically-operated, tricycle-type landing gear with rubber shock discs, a steerable nose wheel, and hydraulic disc brakes. It was powered by an air-cooled, fuel-injected, 200 horsepower, horizontally-opposed, four-cylinder, Lycoming engine driving a 2-blade, variable-pitch, constant-speed McCauley propeller.

According to FAA and airplane maintenance records, the airplane was manufactured in 1980. The airplane's most recent 100-hour inspection was completed on August 13, 2016. At the time of the inspection, the airplane had accrued about 4,690.3 total hours of operation, and the engine had accrued about 100 hours of operation since major overhaul. WRECKAGE AND IMPACT INFORMATIONExamination of the runway revealed the presence of two fresh propeller strike marks and a tire transfer mark, which was perpendicular to and imprinted over one of the propeller strike marks. The strike marks were located 1,747 ft from the beginning of runway 25 and about 4 ft 11 inches to the right of the runway centerline.

Examination of the accident site revealed ground scars and wreckage distribution consistent with the airplane impacting a field in a nose-down attitude and coming to rest against the base of a tree. During the impact sequence, a small tree about 6 ft high was knocked down. Propeller strike marks were visible on about three of the small tree's branches. The leading edge of the right wing displayed crush and compression damage from the tip to about midspan; most of the sheet metal was crushed and accordioned back to the wing spar. The trailing edge of the right wing root also displayed compression damage. The outboard panel of the left wing displayed crush damage and was bent back about 30°.

The engine was separated from its mounting position and was found lying on the ground forward of the left side of the fuselage. The empennage was almost completely separated from the aft fuselage. The right horizontal stabilizer and elevator were wrinkled and displayed impact damage at their outboard ends; the vertical stabilizer and rudder displayed impact damage; and the rudder was partially separated from its mounting position. The landing gear was down, and the flaps were up. Both fuel caps were closed and locked. The fuel tanks were breached, and residual fuel was present in the bottom of the fuel tanks. The throttle control, propeller control, and mixture control were in the full forward positions. The cowl flaps were closed.

Examination of the 2-bladed propeller revealed that a portion of the propeller hub and one propeller blade remained attached to the engine crankshaft flange. The blade that remained attached to the hub exhibited "S" bending, twisting toward the blade face along the longitudinal axis, leading edge gouging, chord-wise scratching, and propeller tip curling of about 150° with an associated area of surface polishing near the curl. The separated blade exhibited chord-wise scratching and black-colored chordwise transfer marks near the propeller tip. The chordwise transfer marks and the tip curling and polishing were consistent with a propeller strike.

The engine remained partially attached to the firewall by fluid hoses and engine control cables. The exhaust tubing was partially crushed, and the muffler was crushed and separated from the engine.

Continuity of the crankshaft to the rear gears and to the valve train was confirmed. Compression and suction were confirmed on all four cylinders. The interiors of the cylinders were observed using a lighted borescope, and no anomalies were noted.

The fuel injector servo was impact-fractured across the throttle bore and separated from the engine. Fuel hoses and control cables remained attached to the servo. The servo throttle control arm was observed in the full throttle position. The servo mixture control arm was observed in the full rich position. The brass plug in the fuel regulator section cover was secure. No damage was noted to the rubber diaphragms or other internal components. The fuel inlet screen was absent of debris.

The fuel flow divider remained attached to the engine, and the injector lines were secure. No damage was noted to the rubber diaphragm or other internal components. The fuel injector nozzles were unobstructed.

The engine-driven fuel pump was impact fractured and partially separated from the engine. No damage was noted to the rubber diaphragms or internal check valves. Liquid with an odor...

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA16FA325