Summary
On October 01, 2016, a Beech 35 (N4836J) was involved in an incident near Lawrence, KS. All 2 people aboard were uninjured. The aircraft sustained substantial damage.
The National Transportation Safety Board determined the probable cause of this incident to be: The flight instructor’s delayed remedial action, which resulted in an unstabilized approach and collision with runway approach lights.
The flight instructor reported that he was conducting primary flight training in a complex, high-performance airplane. On final approach during daylight hours, the runway's precision approach path indicator (PAPI) indicated the airplane was low on the approach path. He advised the student pilot to reduce the rate of decent. He further reported that the student pilot "relaxed his white knuckle grip" and the airplane pitched down "significantly". The flight instructor grabbed the control yoke and applied full throttle, but the airplane struck the runway approach lights during the low altitude recovery. The flight instructor landed the airplane without further incident.
This incident is documented in NTSB report GAA17CA008. AviatorDB cross-references NTSB investigation data with FAA registry records to provide comprehensive safety information for aircraft N4836J.
Accident Details
Probable Cause and Findings
The flight instructor’s delayed remedial action, which resulted in an unstabilized approach and collision with runway approach lights.
Aircraft Information
Registered Owner (Historical)
Analysis
The flight instructor reported that he was conducting primary flight training in a complex, high-performance airplane. On final approach during daylight hours, the runway's precision approach path indicator (PAPI) indicated the airplane was low on the approach path. He advised the student pilot to reduce the rate of decent. He further reported that the student pilot "relaxed his white knuckle grip" and the airplane pitched down "significantly". The flight instructor grabbed the control yoke and applied full throttle, but the airplane struck the runway approach lights during the low altitude recovery. The flight instructor landed the airplane without further incident.
A postaccident examination of the airplane, by the flight instructor, revealed the airplane was trimmed nose down and that the right wing had sustained substantial damage.
The flight instructor reported no preaccident mechanical malfunctions or failures with the airplane that would have precluded normal operation.
Data Source
Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# GAA17CA008