N522LM

Substantial
None

Milholland Kelly DS/N: 76

Accident Details

Date
Friday, October 7, 2016
NTSB Number
CEN17LA015
Location
Livingston, TX
Event ID
20161012X54219
Coordinates
30.679445, -95.013336
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

A total loss of engine power for reasons that could not be determined based on the available information.

Aircraft Information

Registration
N522LM
Make
MILHOLLAND
Serial Number
76
Engine Type
Turbo-shaft
Year Built
1992
Model / ICAO
Kelly DMI2
Aircraft Type
Rotorcraft
No. of Engines
2

Registered Owner (Historical)

Name
AKN INC
Address
6000 DOUGLAS DR N
Status
Deregistered
City
CRYSTAL
State / Zip Code
MN 55429-2314
Country
United States

Analysis

On October 7, 2016, about 1315 central daylight time, a Milholland Kelly D airplane, N522LM, was substantially damaged during a forced landing 1/2 mile north of Livingston Municipal Airport (OOR), Livingston, Texas. The pilot was not injured. The personal flight was conducted under the provisions of 14 Code of Federal Regulations Part 91 without a flight plan. Visual meteorological conditions prevailed. The cross-country flight departed Sport Flyers Airport (27XS), Brookshire, Texas, about 1200, and was en route to OOR.According to the pilot, while approaching OOR for landing, the engine rpms decreased and the engine stopped producing power. He added that there were no indications from the engine or the engine gauges prior to the sudden power loss. During the forced landing to the field, the landing gear collapsed and partially separated from the fuselage. The lower wings, fuselage, and firewall were substantially damaged.

An examination of the engine revealed that the left magneto was not producing spark. Further examination of the engine and related systems revealed no additional mechanical anomalies that would have precluded normal operations.

The left magneto was placed on a test machine and brought to operating speed. Each of the four ignition leads produced spark; however, at times the spark was intermittent. Further examination of the magneto revealed a greyish color on the points, consistent with failure of the capacitor. The technician remarked that a magneto could test within expected parameters but when it got hot during normal engine operations, it could fail.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN17LA015