N5499Z

Substantial
None

PIPER PA22S/N: 22-9285

Accident Details

Date
Wednesday, December 28, 2016
NTSB Number
CEN17LA062
Location
Piedmont, MO
Event ID
20161229X93022
Coordinates
37.124443, -90.714996
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The pilot’s descent below glidepath, which resulted in the airplane’s impact with power lines.

Aircraft Information

Registration
N5499Z
Make
PIPER
Serial Number
22-9285
Engine Type
Reciprocating
Year Built
1962
Model / ICAO
PA22PA22
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
LIGONS DEWAYNE D
Address
RR 2 BOX 2099
Status
Deregistered
City
ELLSINORE
State / Zip Code
MO 63937-9532
Country
United States

Analysis

On December 27, 2016, about 1830 central standard time, a Piper PA22-108 airplane, N5499Z, impacted a power line and terrain near Piedmont, Missouri. The private rated pilot was not injured and the airplane was substantially damaged during the accident. The airplane was registered to and operated by a private individual under the provisions of 14 Code of Federal Regulations Part 91 as a personal flight. Visual meteorological conditions prevailed at the time.

The pilot reported that he had performed several touch-and-go landings at another airfield, and then returned to the Piedmont Municipal Airport ( KPYN), for additional touch-and-go's. As he approached the runway for the third landing, he added throttle to adjust his glide path; however, the engine did not respond. He added that the engine continued to run, but did not have enough power to maintain altitude. The airplane continued to descend and then the airplane's landing gear caught a power line. The airplane impacted terrain, coming to rest inverted about a half mile short of the runway.

The Federal Aviation Administration (FAA) inspector found that substantial damage was noted to the airplane's fuselage and wings. Fuel was present on site. Further examination of the airplane revealed that control continuity was confirmed to the respective flight and engine controls. When rotated by hand, engine continuity and compression was established on each cylinder. Inspection of the propeller blade tips found they were bent forward; leading edges were gouged and displayed cord wise scoring. No pre-impact abnormalities were noted during the airframe or engine examination.

The automated weather observation facility located at the Poplar Bluff Municipal Airport (KPOF) located 29 miles southeast of the accident site recorded at 1753, wind from 170 degrees at 3 knots, 10 miles visibility, a clear sky, temperature 40 degrees Fahrenheit (F), dew point 34 F, and a barometric pressure of 30.25 inches of mercury.

The carburetor icing probability chart included in Federal Aviation Administration Special Airworthiness Information Bulletin No. CE-09-35, Carburetor Icing Prevention, indicated that the airplane was operating in an area that was associated with a serious risk of carburetor ice formation at cruise power settings.

The pilot stated that he did not use carburetor heat on the approach; adding that the POH (pilot's operating handbook) doesn't call for the use of carburetor heat when at reduced power settings, only at reduced power settings when carburetor icing conditions are present.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN17LA062