N415HC

Substantial
None

QUICKSILVER GT-400 R503S/N: 1504

Accident Details

Date
Sunday, January 1, 2017
NTSB Number
CEN17LA079
Location
New Braunfels, TX
Event ID
20170117X42903
Coordinates
29.641387, -98.202774
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The partial loss of engine power due to a loose spark plug. Contributing to the accident was the pilot's improper preflight inspection of the airplane.

Aircraft Information

Registration
Make
QUICKSILVER
Serial Number
1504
Engine Type
2-cycle
Year Built
2006
Model / ICAO
GT-400 R503
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
1
FAA Model
GT-400 R503

Registered Owner (Current)

Name
GRABIEC RAYMOND T
Address
PO BOX 3617
City
LANDERS
State / Zip Code
CA 92285-0617
Country
United States

Analysis

On January 1, 2017, about 1130 central standard time, a Quicksilver GT-400 R503 experimental light sport airplane, N415HC, impacted power lines during a forced landing following a partial loss of engine power near New Braunfels, Texas. The sport pilot, who was the sole occupant, was not injured, and the airplane sustained substantial damage. The airplane was registered to and operated by a private individual as a 14 Code of Federal Regulations Part 91 personal flight. Visual meteorological conditions prevailed at the time of the accident and a flight plan was not filed. The local flight departed a private airstrip about 1110.

According to the pilot/owner, about 15 minutes into the pleasure flight, the engine began "sputtering" and losing power. The pilot attempted to correct the problem by adjusting the throttle and applying engine primer. The attempts were unsuccessful in restoring engine power. The pilot then identified a field for a forced landing. During the forced landing, the right main landing gear struck a power line. After impacting the power line, the airplane flipped inverted, and dropped about 20 feet onto a carport rooftop. The pilot exited the airplane.

Examination of the airplane by Federal Aviation Administration inspectors revealed both wings were bent and the wing fabric was damaged. No visual anomalies with the engine were noted.

After the airplane was recovered from the carport, the pilot and a few friends examined the airplane and systems. The pilot noticed that one of the four engine spark plugs was loose in the cylinder. The pilot determined that the loose spark plug led to a loss of compression and partial loss of engine power during the accident flight. The pilot's safety recommendation, as noted in the pilot/operator accident report, stated "closer inspection of checking spark plugs before flight."

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN17LA079