Accident Details
Probable Cause and Findings
The pilot's failure to maintain proper altitude resulting in a collision with water for reasons that could not be determined based on the available information.
Aircraft Information
Registered Owner (Historical)
Analysis
HISTORY OF FLIGHTOn February 27, 2017, about 1033 central standard time, a Bell 407 helicopter, N1371, was destroyed when it impacted marshy water 15 miles southwest of Houma, Louisiana (HUM). The commercial pilot was fatally injured. The repositioning flight was operated by Westwind Helicopters under the provisions of Title 14 Code of Regulations (CFR) Part 91. Visual meteorological conditions prevailed throughout the area and a company flight plan was activated. The flight originated at 1014 from offshore oil platform South Timbalier ST37, Gulf of Mexico.
Before the accident flight, the helicopter had completed a 14 CFR Part 135 passenger flight from HUM to ST37, dropping off 2 passengers. The passengers reported that the flight to ST37 was normal. According to the operator, the pilot was to return the helicopter to HUM for a minor repair of an engine cowling fastener. The pilot was the only person on board for the approximate 30-minute flight to HUM.
The helicopter was equipped with an on-board flight tracking system (Sky Connect). After takeoff from ST37, six flight path data points were recorded at 2-minute intervals and showed the helicopter on a northwest heading. Sky Connect data showed the flight path of the helicopter flying direct toward HUM on a northwest heading. Sky Connect Flight Path Data Points:
1 Heading 207 degrees, altitude 108 feet, ground speed 8 knots (ST37 Departure)
2 Heading 337 degrees, altitude 728 feet, ground speed 148 knots
3 Heading 336 degrees, altitude 699 feet, ground speed 144 knots
4 Heading 336 degree, altitude 486 feet, ground speed 144 knots
5 Heading 336 degrees, altitude 548 feet, ground speed 150 knots
6 Heading 336 degrees, altitude 374 feet, ground speed 148 knots (Last Recorded Point)
Figure. Sky Connect Flight Path
The figure shows the helicopter's altitude, heading, and ground speed; ST37 is located at the right of the figure. The last Sky Connect data point was at 1024, indicating an altitude of 374 ft and ground speed of 148 knots. Sky Connect issued an "Overdue" alarm at 1033. At 1103, company flight monitoring personnel dispatched a search helicopter, and the wreckage was found at 1135 about 15 miles south-southeast of HUM.
There were no reported witnesses to the accident. There were no radio or distress calls heard from the helicopter, and the helicopter's Sky Connect emergency button was not activated. PERSONNEL INFORMATIONThe pilot held a commercial pilot certificate with rotorcraft-helicopter and instrument ratings. He was hired by Westwind Helicopters on July 17, 2016. His total flight time as of February 27, 2017 was 2,266 hours, all of which was in light helicopters. His total flight time in the accident helicopter make and model was 120 hours. He had flown 140 flight hours in single-engine helicopters in the 90 days before the accident. According to pilot training records provided by the operator, the pilot was current and qualified in offshore Part 135 flight operations. His most recent Federal Aviation Administration (FAA) second-class medical certificate was issued in June 2016 with no limitations. AIRCRAFT INFORMATIONWestwind Helicopters leased the helicopter, serial number (S/N) 53182, from GM Leasing in April 2015. It had a total airframe time of 9,146.8 hours at the time of the accident. The helicopter was equipped with an Allison 250C47B turbo shaft engine (S/N CAE847222) with a total time of 15,510.6 hours. According to maintenance records provided by the operator, the most recent 100-hour inspection was completed on February 16, 2017, at 9,125.5 airframe hours.
Maintenance records indicated compliance with all required scheduled maintenance inspections, applicable service bulletins, and applicable airworthiness directives. A review of the maintenance logbooks by the NTSB IIC did not reveal any uncorrected scheduled or unscheduled maintenance actions. METEOROLOGICAL INFORMATIONAt 0950, the weather observation at HUM included wind from 150° at 12 knots gusting to 17 knots, visibility 5 statute miles with haze, scattered clouds at 1,000 ft and a broken ceiling at 2,200 ft, temperature 24°C, dew point 21°C, and an altimeter setting of 30.12 inches of mercury.
The search pilot reported that the conditions in the area of the accident site included 5-7 miles visibility with ceilings above 700 ft about 1130. AIRPORT INFORMATIONWestwind Helicopters leased the helicopter, serial number (S/N) 53182, from GM Leasing in April 2015. It had a total airframe time of 9,146.8 hours at the time of the accident. The helicopter was equipped with an Allison 250C47B turbo shaft engine (S/N CAE847222) with a total time of 15,510.6 hours. According to maintenance records provided by the operator, the most recent 100-hour inspection was completed on February 16, 2017, at 9,125.5 airframe hours.
Maintenance records indicated compliance with all required scheduled maintenance inspections, applicable service bulletins, and applicable airworthiness directives. A review of the maintenance logbooks by the NTSB IIC did not reveal any uncorrected scheduled or unscheduled maintenance actions. WRECKAGE AND IMPACT INFORMATIONGeneral
The wreckage was found in shallow marsh waters south of Timbalier Bay, about 15 miles south-southeast of HUM. The wreckage was recovered and transported to a salvage facility in Baton Rouge, Louisiana. The recovered portions included the main fuselage, tailboom, the main rotor drive system, main rotor blades, engine, tail rotor blades and tail rotor gearbox, and landing gear with skid-mounted float assembly.
Detailed examinations of the recovered components were conducted under the supervision of the NTSB investigator-in-charge. The FAA, Westwind Helicopters, Rolls Royce, and Bell Helicopter participated in the airframe examinations at Southern Aircraft Recovery on March 2-3, 2017. The Rolls-Royce engine was examined under the supervision of the FAA on March 3, 2017, at Arrow Aviation, Broussard, Louisiana. The Engine Control Unit (ECU) was transported to Triumph Engine Controls in West Hartford, Connecticut, for data extraction. The following are summaries of the examinations.
Airframe
The airframe was destroyed by impact forces upon water contact, breaking into several pieces. Airframe deformations were consistent with a slightly nose low and left skid down orientation at the time of impact. The left forward Dzus fastener on the engine cowling that was reported loose at the ST37C platform was missing, and the cowling mounting hole was found fractured. The left side of the helicopter exhibited more damage than the right side, including doors, landing gear, and cockpit and nose area. The tailboom remained connected to the aft fuselage and the aft fuselage was separated from the aft engine firewall bulkhead. The tailboom was relatively intact with two slight bends to the left. The vertical fin exhibited a tail rotor strike to its bottom surface, consistent impact forces occurring after the tail rotor gearbox departed its mounting location.
The skid-mounted float system was not deployed.
Rotors
All four main rotor blades exhibited spar and afterbody damage consistent with impact forces, but no spar fractures were observed. The top blade surface balance pocket weights located near the blade tips' leading edges were all intact, remaining firmly attached to the blade spars. The bottom blade surface balance pocket weights located near the blade tips' trailing edges had all departed from their mounting pockets in the blades afterbody surfaces.
All four main rotor yoke arms were significantly damaged from impact forces, exhibiting delamination and fractures of the composite yoke flexure structure. All hub bearings were damaged consistent with overtravel. Up-stops and down-stops were significantly damaged, consistent with impact forces.
Both tail rotor blades remained connected to their respective yoke arms. Both blades were relatively intact with one blade exhibiting trailing edge blade tip skin delamination consistent with impact forces.
No pre-impact anomalies were found in the main or tail rotor systems and the damages found were consistent with rotation at impact.
Flight Controls and Hydraulics
The cockpit area was destroyed by impact forces. The helicopter was equipped with single controls at the pilot's station. The vertical tunnel where four vertical flight control tubes transit was found fractured consistent with impact at top and bottom surfaces. All four control tubes exhibited overload fractures at the top of the vertical tunnel and the right cyclic pitch control tube was found fractured in overload about 1 ft from the bottom of the tube. The cyclic was intact and remained connected to the control system. Cyclic movement revealed corresponding movement of the vertical control tubes. The collective was fractured at its cast base, consistent with impact forces. The collective jackshaft was intact but displaced due to extensive cockpit damage. Control linkages to the main rotor servos were found intact. All three main rotor servos and mounting support structures were intact, including intact nut and locking tabs at the spool valve wire drive to spool control lever connections.
Tail rotor control system fractures were found at various locations due to airframe impact damage. The tail rotor pitch control was found intact.
The hydraulic manifold was found intact and the hydraulic reservoir was full of hydraulic fluid. Both the pressure line to the manifold and the rotor brake hydraulic line were found fractured, consistent with overload forces. The bypass pop-out buttons for both the pressure and return lines were not extended. The hydraulic pump remained attached to the main transmission, but the elbow pressure fitting was found fractured consistent with impact forces.
No pre-impact anomalies were found in the flight control or hydraulic systems.
Drive System
The mast was intact and the chip detectors were clea...
Data Source
Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN17FA112