N2492U

Substantial
Minor

CESSNA 172S/N: 17250092

Accident Details

Date
Friday, July 7, 2017
NTSB Number
ERA17LA234
Location
Cape Coral, FL
Event ID
20170707X12032
Coordinates
26.637222, -81.976112
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
1
Uninjured
0
Total Aboard
1

Probable Cause and Findings

A total loss of engine power due to fuel contamination with water and the pilot's inadequate preflight inspection that detected, but did not fully resolve, the water contamination of the fuel system.

Aircraft Information

Registration
N2492U
Make
CESSNA
Serial Number
17250092
Engine Type
Reciprocating
Year Built
1963
Model / ICAO
172C172
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
GOSS CHADWICK D
Address
727 KARI CIR
Status
Deregistered
City
LEHIGH ACRES
State / Zip Code
FL 33974-2640
Country
United States

Analysis

On June 7, 2017, about 0950 eastern daylight time, a Cessna 172D airplane, N2492U, lost engine power over Cape Coral, Florida, and was substantially damaged during a forced landing. The pilot sustained minor injuries. Visual meteorological conditions prevailed and no flight plan was filed for the local flight, which originated from Page Field Airport (FMY), Fort Myers, Florida. The personal flight was conducted under the provisions of Title 14 Code of Federal Regulations Part 91.According to the pilot, prior to the flight he performed a preflight inspection and sumped the fuel tanks several times. He said that he only observed a small amount of water drain from the tanks. He performed an engine run up and no anomalies were observed prior to takeoff. After takeoff while in cruise flight at an altitude of 1,200 ft above the ground (agl), the pilot observed a loss of engine power. He immediately changed his course to return to the departure airport and applied carburetor heat to regain power. The engine continued to run rough at a decreased power setting, but the airplane maintained an altitude of 800 ft agl. As he planned for an emergency landing, the engine lost all power. He notified air traffic control that he was "going down" and began an emergency descent. The airplane struck power lines and collided with the ground nose first. The pilot exited the airplane and waited for emergency services.

The Federal Aviation Administration (FAA) inspector arrived on scene about 4 hours after the accident and noted that the airplane was inverted in a parking lot. During the examination of the airplane he observed that the nose of the airplane was crush aft, the engine was crushed against the firewall and there was buckling throughout the fuselage. A mixture of water and fuel was observed dripping out of the right wing fuel cap. The inspector estimated about 2 gallons of water flowed from the fuel tanks. He contacted the fire chief on scene and asked if water was sprayed on the airplane; the fire chief responded "no" and went on to say that "the pilot was also looking at the water dripping from the tank." After the airplane was removed it was discovered that the fuel caps had an extensive amount of rust on both fuel ports.

An examination of the engine revealed impact damage signatures. The two blade, fixed pitch propeller remained attached to the crankshaft and displayed impact damage signatures to both of the blades. The crankshaft propeller flange remained partially attached to the rest of the crankshaft; the crankshaft was cracked aft of the propeller flange which was consistent with impact damage. The propeller was rotated by hand and camshaft, crankshaft, and valve train continuity to the rear accessory section of the engine was observed. Due to damage to the engine an engine test-run was not attempted. The magnetos, and the ignition harness were impact damaged and were unable to provide any useful information. The engine assembly did not reveal any anomalies within the drivetrain that would have precluded normal operation.

Examination of the carburetor revealed a significant amount of corrosion noted within the carburetor; there were several large flakes of corroded material at the bottom of the fuel bowl and one flake was located within the mixture control housing.

Examination of the airframe revealed flight control continuity to all of the flight surfaces and flight controls. Examination the airframe did not reveal any anomalies that would have precluded normal operation.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA17LA234