N210SQ

Substantial
Minor

BRADLEY RODERICK W MURPHY RENEGADES/N: REN 575

Accident Details

Date
Monday, August 14, 2017
NTSB Number
ERA17LA276
Location
Guilford, CT
Event ID
20170815X73929
Coordinates
41.280834, -72.673332
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
1
Uninjured
0
Total Aboard
1

Probable Cause and Findings

A total loss of engine power for reasons that could not be determined based on the available evidence.

Aircraft Information

Registration
Make
BRADLEY RODERICK W
Serial Number
REN 575
Engine Type
Reciprocating
Year Built
1995
Model / ICAO
MURPHY RENEGADEFK9
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
2
FAA Model
MURPHY RENEGADE

Registered Owner (Current)

Name
BRADLEY RODERICK W
Address
44 HIDDEN LN
City
GUILFORD
State / Zip Code
CT 06437-2849
Country
United States

Analysis

On August 14, 2017, about 1620 eastern daylight time, an experimental amateur-built Murphey Renegade, N210SQ, was substantially damaged during a forced landing near Guilford, Connecticut. The airline transport pilot received minor injuries. The airplane was registered to and operated by the pilot as a Title 14 Code of Federal Regulations Part 91 personal flight. Visual meteorological conditions prevailed at the time of the accident, and no flight plan was filed for the flight that departed Tweed-New Haven Airport (HVN), New Haven, Connecticut, about 1550.According to the pilot, the accident flight was the first flight after the carburetors were inspected, repaired, and reinstalled on the engine. During the preflight inspection, he checked for water in the fuel, which was automotive fuel with 5% ethanol, and noted none. Review of air traffic control communication transcripts revealed that about 30 minutes after departing HVN the pilot declared an emergency to the HVN tower controller and stated that his engine had lost power. He advised the tower controller that he was about 10 miles east of the airport and was going to perform a forced landing to the local fairgrounds. While on approach, the airplane struck powerlines and came to rest in a field.

According to the Federal Aviation Administration (FAA) inspector who responded to the accident site, the forward section of the fuselage was substantially damaged. The propeller was not damaged and there was fuel present in the fuel tanks.

An examination of the engine revealed that crankshaft continuity was confirmed by rotating the propeller by hand, and thumb compression was established on all cylinders. The spark plugs and ignition system were examined, and no anomalies were noted. The fuel pump was examined, and no anomalies were noted. The carburetors were partially disassembled, the diaphragms were intact, the main jet and idle jets were not blocked, and no corrosion was noted on those parts. The left idle mixture screw had a small amount of corrosion, otherwise, there were no other anomalies with the carburetors.

According to the pilot, he had the carburetors inspected and repaired twice as a result of a "rough running engine." Once in February 2017 and then again in July 2017. Both times, the pilot reinstalled the carburetors and noted that the engine ran "normal." The pilot stated that there was evidence of water contamination both times, and once, one of the fuel jets in the carburetors was a blue/green color "because of corrosion."

According to the maintenance work orders, a maintenance shop performed the manufacturer's 200-hour carburetor service requirement and the 5-year rubber replacement requirements in February 2017. Then, in July 2017, maintenance personnel indicated that the carburetor was inspected and "found idle circuit was corroded. Cleaned, performed ground run-up – tested good."

In a letter to the maintenance facility that performed the carburetor maintenance, the pilot noted on-going issues with the engine. The following is what he stated in his letter sent in July 2017:

318 hours – rough running [engine] replaced idle jets

331 hours – new spark plugs

340 hours – engine would not start, replaced both ignition modules

342 hours – rough running [engine], cleaned idle jets

373 hours – loss of power after takeoff, sent carb[ureters] to maintenance shop for rebuild

395 hours – rough running [engine], bought new idle jets

395 hours – weighed floats, replaced spark plugs, check main pistons for free movement, checked air cleaners.

"Rough running continues, spark plugs badly sooted."

According to the pilot, on the day of the accident the airplane had accumulated 410 hours of total time.

According to Rotax Service Instruction "Selection of Suitable Operating Fluids for Rotax Engine 912 and 914 series," automotive fuel with up to 10% of ethanol was permitted to be used for operation.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA17LA276