N52PD

Unknown
None

ENSTROM F 28FS/N: 807

Accident Details

Date
Tuesday, August 22, 2017
NTSB Number
WPR17IA198
Location
Glendale, AZ
Event ID
20170822X63531
Coordinates
33.526943, -112.295280
Aircraft Damage
Unknown
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

An internal failure of the turbo-compressor, which resulted in oil leaking into the turbo-compressor’s exhaust.

Aircraft Information

Registration
Make
ENSTROM
Serial Number
807
Engine Type
Reciprocating
Year Built
1996
Model / ICAO
F 28FEN28
Aircraft Type
Rotorcraft
No. of Engines
1
Seats
3
FAA Model
F-28F

Registered Owner (Current)

Name
AVIATION ENDEAVORS LLC
Address
10685B HAZELHURST DR # 32654
City
HOUSTON
State / Zip Code
TX 77043-3238
Country
United States

Analysis

On August 22, 2017, about 0904 mountain standard time, an Enstrom F-28F helicopter, N52PD, experienced smoke coming from the engine cowling area after touchdown at the Glendale Municipal Airport (GEU) Glendale, Arizona. The certified flight instructor and student pilot were not injured, and the helicopter was not damaged. The helicopter was registered to and operated by Airwest Aviation Academy LLC under the provisions of Title 14 Code of Federal Regulations Part 91, as an instructional flight. Visual meteorological conditions prevailed, and no flight plan had been filed. The local flight departed GEU about 0820.

The flight instructor reported that at the time of the incident, the student was practicing hovering autorotations. Several had been accomplished without incident. During the last one, the engine appeared to have stalled, but sounded as if it were running rough when the cockpit filled with smoke. The helicopter was on the ground and the flight instructor secured the cockpit and both he and the student evacuated the helicopter with the engine still running and smoke coming out of the right side air scoop. About five minutes later, the engine stopped running.

Postincident examination of the helicopter revealed that no fire or other related damage was present. Maintenance personnel reported that the source of the smoke appeared to have originated from the failure of an internal oil seal within the turbocharger-compressor that leaked oil into the turbocharger-compressor's exhaust system. No further examination or repair was accomplished and the turbocharger was replaced.

Further examination identified that the V-clamp assembly that was installed on the turbo-compressor exhaust was damaged. The V-clamp assembly was removed and sent to the National Transportation Safety Board Material Laboratory, Washington DC for further examination. The examination of the V-clamp assembly revealed that the strap portion of the assembly contained cracks on three of the four spot welds that emanated from the outer face of the strap. The edge of the strap portion exhibited evidence of bending deformation on both sides of the assembly. In the deformed areas, the distance between the edge of the retainer and the edge of the strap, were smaller when compared to other non-deformed areas. Microscopic examination of the longest crack revealed that a fatigue crack emanated from the outer surface of the strap. The damage to the V-clamp was unrelated to the source of the smoke.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# WPR17IA198