N8695H

Substantial
None

NORTH AMERICAN NAVION AS/N: NAV-4-695

Accident Details

Date
Sunday, August 27, 2017
NTSB Number
WPR17LA191
Location
Fortuna, CA
Event ID
20170828X12800
Coordinates
40.558612, -124.148887
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

A total loss of engine power for reasons that could not be determined because postaccident examination of the engine revealed no evidence of any preaccident mechanical malfunctions or failures that would have that would have precluded normal operation.

Aircraft Information

Registration
Make
NORTH AMERICAN
Serial Number
NAV-4-695
Engine Type
Reciprocating
Model / ICAO
NAVION AT2
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
5
FAA Model
NAVION A

Registered Owner (Current)

Name
MOAK ERIC DAVID
Address
627 W LACEY AVE
City
HAYDEN
State / Zip Code
ID 83835-9736
Country
United States

Analysis

On August 27, 2017, about 1620 Pacific daylight time, a North American Navion A airplane, N8695H, experienced a total loss of engine power during the initial climb from Rohnerville Airport, Fortuna, California. The private pilot was not injured; the airplane sustained substantial damage to the firewall during the forced landing. The airplane was registered to and operated by the pilot as a Title 14 Code of Federal Regulations Part 91 personal flight. Visual meteorological conditions prevailed and no flight plan had been filed for the local flight which departed from Fortuna about 1615.

The pilot stated that he departed with about 10-12 gallons of fuel on board. After the airplane reached about 1,000 ft above ground level (agl), the engine experienced a total loss of power. He attempted to return back to the airport, but was unable to maintain altitude and he made an off-airport landing in a pasture about .5 miles from the runway at Fortuna.

A Federal Aviation Administration (FAA) certificated airframe and powerplant mechanic completed a post accident examination under the auspice of an FAA inspector. The inspector noted that the original engine for this airplane was replaced by a Teledyne Continental Motors IO-470H which was installed in June 2003. The spark plugs were removed from all cylinders revealing no signs of deterioration, wear or oil/carbon fouling. Continuity was established for each magneto, which produced spark at each cylinder. A borescope inspection of each cylinder revealed no evidence of excessive wear, deterioration, broken rings, or broken valves.

The FAA inspector further stated that he observed fuel in the left, right, and main tanks. He sumped samples from each tank disclosing that there was no debris or water visible. Disassembly of the fuel manifold revealed a clean screen; there was no fuel visible. The mechanic removed the fuel inlet supply line to the fuel manifold and activated the electric fuel boost pump. Fuel flowed normally out of the inlet supply line from the tank that was selected, all of which were selected. The reason for the loss of power was not determined.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# WPR17LA191