N930WN

Substantial
None

BOEING 737 7H4S/N: 36636

Accident Details

Date
Monday, October 2, 2017
NTSB Number
DCA18CA001
Location
Chicago, IL
Event ID
20171003X23920
Coordinates
41.786388, -87.745277
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
84
Total Aboard
84

Probable Cause and Findings

the mechanical failure of the tugs fuel governor, which made it difficult for the ramp agent to stop the tug. Contributing to the accident was the lack of guidance on how ground personnel were to handle vehicle malfunctions.

Aircraft Information

Registration
Make
BOEING
Serial Number
36636
Engine Type
Turbo-fan
Year Built
2009
Model / ICAO
737 7H4
Aircraft Type
Fixed Wing Multi Engine
No. of Engines
2
Seats
143
FAA Model
737-7H4

Registered Owner (Current)

Name
WILMINGTON TRUST COMPANY TRUSTEE
Address
1100 N MARKET ST
City
WILMINGTON
State / Zip Code
DE 19890-1805
Country
United States

Analysis

On October 2, 2017, at about 0840 CDT, Southwest Airlines flight 681, Boeing B737-700, N930WN, was struck by an unmanned tug while boarding was ongoing at Chicago Midway Airport (KMDW), Chicago, Illinois. There were no injuries to the 84 passengers and crew onboard. The airplane received substantial damage to the lower fuselage skin, frames and stringers over an area about 3 feet by 3 feet. The flight was operating under 14 Code of Federal Regulation Part 121 as a scheduled passenger flight from KMDW to Omaha Airport (KOMA), Omaha, Nebraska.

A ramp agent was driving a covered baggage tug with two baggage carts in tow between Gates B22 and B24 when the tug made contact with two staged baggage carts. The ramp agent jumped off the tug as the tug continued to accelerate forward. The now unmanned baggage tug struck additional ground support equipment before striking the fuselage of the accident airplane at Gate B22. The ramp agent stated afterwards that he could not get the tug to stop and thought running the tug into the staged baggage carts would stop or at least slow the tug down.

Examination of the baggage tug after the event revealed there was a mechanical failure of the fuel governor which resulted in the runaway. The runaway could have been stopped by either turning the ignition key off or using the manual shut down lever on the front cover. There was no guidance in the Ground Operations Training Manual related to how ramp personnel should handle mechanical failures of ground support equipment.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# DCA18CA001