N47831

Destroyed
Fatal

PIPER PA 32S/N: 32-7840014

Accident Details

Date
Wednesday, November 8, 2017
NTSB Number
ERA18FA016
Location
Morrison, TN
Event ID
20171107X13608
Coordinates
35.652778, -85.916389
Aircraft Damage
Destroyed
Highest Injury
Fatal
Fatalities
2
Serious Injuries
0
Minor Injuries
0
Uninjured
0
Total Aboard
2

Probable Cause and Findings

The pilots' loss of control during a missed approach in night instrument meteorological conditions as a result of spatial disorientation.

Aircraft Information

Registration
N47831
Make
PIPER
Serial Number
32-7840014
Engine Type
Turbo-shaft
Year Built
1978
Model / ICAO
PA 32M600
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
A W STILES CONTRACTORS INC
Address
286 BASS LN
Status
Deregistered
City
MCMINNVILLE
State / Zip Code
TN 37110-4360
Country
United States

Analysis

HISTORY OF FLIGHTOn November 7, 2017, about 1845 central standard time, a Piper PA-32-300, N47831, was destroyed after it impacted terrain near Morrison, Tennessee. The flight instructor and private pilot were fatally injured. The airplane was privately owned and operated as a Title 14 Code of Federal Regulations Part 91 instructional flight. Night instrument meteorological conditions (IMC) prevailed, and an instrument flight rules (IFR) flight plan was filed for the flight, which originated from Monroe County Aeroplex Airport (MVC), Monroeville, Alabama, about 1625, and was destined for Warren County Memorial Airport (RNC), McMinnville, Tennessee.

According to a friend of the private pilot, who was also a pilot, he and the private pilot were fishing in Florida the day before the accident. The flight instructor flew to Destin Executive Airport (DTS), Destin, Florida, the day of the accident to pick up the pilot. The friend stated that he tried to convince the private pilot to drive back from Florida with him instead of flying since the weather "was so bad."

A fuel receipt from a fixed based operator at DTS indicated that the airplane was fueled with 27 gallons of fuel before it departed for MVC, an intermediate stop on the way to RNC.

According to air traffic control data provided by the Federal Aviation Administration (FAA), the controller cleared the airplane for the RNAV Runway 23 approach to RNC and issued the airplane a frequency change to the RNC common traffic advisory frequency (CTAF). The pilots conducted a missed approach and subsequently requested a clearance to Upper Cumberland Regional Airport (SRB), Sparta, Tennessee. The controller radar-identified the airplane, instructed the pilots to climb the airplane to 5,000 ft mean sea level (msl), and cleared the airplane to SRB. In addition, the controller issued the weather for SRB, which included overcast clouds at 300 ft above ground level (agl). One of the pilots asked the controller to verify the overcast cloud conditions at SRB and indicated that he would tune the radio to the SRB automated weather observation service (AWOS) broadcast. About this time, the radar target reached about 4,800 ft and began a right descending turn. While in the descent, one of the pilots declared "mayday" and the target continued to descend at a maximum descent rate about 4,500 ft per minute until radar contact was lost.

According to witnesses, the engine was "loud" and they reported hearing it "throttle up" before they heard the impact. One witness stated that the airplane "sounded like it was doing crazy maneuvers." PERSONNEL INFORMATIONAccording to FAA airman records, the flight instructor held a commercial pilot certificate with ratings for airplane multiengine land, airplane single-engine land, glider, rotorcraft-gyroplane, and instrument airplane. In addition, he held a flight instructor certificate with ratings for airplane single-engine, glider, rotorcraft-gyroplane, and instrument airplane. He received a BasicMed certificate on June 22, 2017. In August 2016, he reported 8,312 total hours of flight experience. According to the flight log found in the airplane, the flight instructor had accumulated about 2 hours of flight time in the accident airplane since October 6, 2017.

According to FAA airman records, the private pilot held a private pilot certificate with a rating for airplane single-engine land. He was issued a third-class medical certificate on November 3, 2016. On the application for that certificate, he reported 16 total hours of flight experience; all 16 hours were within the previous 6 months. According to a flight log found in the wreckage, the pilot had accumulated about 24 hours of flight time in the accident airplane since October 6, 2017. According to a friend of the pilot, the pilot was scheduled to take his instrument rating practical test on November 27, 2017. In addition, the pilot "had about 40 hours of actual instrument time since he flew the airplane everywhere for work and would take the flight instructor with him." AIRCRAFT INFORMATIONAccording to FAA airworthiness records, the airplane was manufactured in 1978 and was purchased by the private pilot in September 2016. It was powered by a Lycoming IO-540 series, 300-horsepower engine equipped with a Hartzell constant-speed propeller. According to airplane maintenance logbooks, the most recent annual inspection was completed on May 1, 2017, at a total time of 4,133 hours and a Hobbs time of 1,549.3 hours. According to a flight log located in the wreckage, at the time of departure on the accident flight, the airplane Hobbs meter indicated 1,781.3 hours. METEOROLOGICAL INFORMATIONThe 1845 recorded weather observation at RNC, about 5 miles northeast of the accident site, included wind from 350° at 6 knots, 2 1/2 miles visibility, mist, overcast clouds at 500 ft agl temperature 12°C, dew point 11°C, and an altimeter setting of 30.09 inches of mercury.

The 1845 recorded weather observation at SRB, about 31 miles northeast of the accident site, included wind from 340° at 6 knots, 8 miles visibility, overcast ceiling at 400 ft agl, temperature 10°C, dew point 10°C, and an altimeter setting of 30.08 inches of mercury.

According to an NTSB meteorologist, the observations surrounding the accident time indicated mainly IFR conditions with brief periods of low IFR (LIFR) conditions in mist. No precipitation was observed around the accident time.

The pilot received Leidos weather briefings at 0605 and 0953 for planned flights on the day of the accident, but not for the accident flight. The pilot had additional contact with Leidos at 0838 and 1556. During the 1556 contact with Leidos, the accident flight route was discussed, and the pilot mentioned that he already had the weather conditions for the proposed destination and that the conditions were LIFR. The accident pilot did not request any weather information or forecast information during the 1556 briefing. All of the standard weather forecast and current weather information were provided to the accident pilot during the 0605 and 0953 briefings.

According to the Astronomical Applications Department at the United States Naval Observatory, sunset was at 1642, the end of civil twilight was at 1709, and moonrise was at 2015. The phase of the moon was waning gibbous, with 83% of the moon's visible disk illuminated. AIRPORT INFORMATIONAccording to FAA airworthiness records, the airplane was manufactured in 1978 and was purchased by the private pilot in September 2016. It was powered by a Lycoming IO-540 series, 300-horsepower engine equipped with a Hartzell constant-speed propeller. According to airplane maintenance logbooks, the most recent annual inspection was completed on May 1, 2017, at a total time of 4,133 hours and a Hobbs time of 1,549.3 hours. According to a flight log located in the wreckage, at the time of departure on the accident flight, the airplane Hobbs meter indicated 1,781.3 hours. WRECKAGE AND IMPACT INFORMATIONThe main wreckage was located in a field at an elevation of 1,030 ft msl about 1,500 ft from the last radar return. The airplane impacted the field and came to rest about 100 ft beyond the initial impact point on a 040° heading. A 2.5-ft indentation was noted at the initial impact point. All major components of the airplane were located in the vicinity of the main wreckage.

The wreckage came to rest upright and was partially consumed by postimpact fire. Flight control continuity was confirmed from all flight control surfaces to the flight controls in the cockpit through cuts made to facilitate recovery. The cockpit area was damaged. The electric HSI remote gyro was removed from the airframe, disassembled, and rotational scoring was noted on the housing. The right wing exhibited leading edge damage and sections were consumed by postimpact fire. The inboard section of the right flap remained attached to the right wing. The outboard right aileron remained attached to the right wing at the outboard hinge. The remainder of the right aileron was consumed by fire. The left wing was impact-separated at the spar box and remained attached at the forward fuselage attach point. The leading edge exhibited impact damage and skin separation. Thermal damage was noted on the inboard approximate 5-ft section of the left wing. The outboard approximate 8-ft section of the left wing was impact-separated and located in the vicinity of the main wreckage. The vertical stabilizer remained attached to the fuselage. The rudder remained attached to the vertical stabilizer. The stabilator remained attached at all attach points. The right side of the stabilator was deformed in the positive direction. The trim tab remained attached to the stabilator at all attach points. The trim tab control was measured and corresponded to the near full nose up position.

The propeller remained attached to the crankshaft flange. All three propeller blades remained attached to the hub. There was leading edge damage noted along all of the blades

The engine remained attached to the firewall but was removed to facilitate examination. Engine crankshaft continuity was confirmed from the propeller flange to the accessory section of the engine. All cylinders remained attached to the crankcase and thumb compression and suction were obtained on all cylinders. The rocker box covers were removed and no anomalies were noted with the valve springs and rocker arms. Valve train continuity was confirmed when the crankshaft was rotated through 360°. Both magnetos remained attached to the engine, but were partially consumed by fire. The oil filter was removed and disassembled. The filter was charred and absent of metallic debris. The oil suction screen was removed from the engine and free of debris. The vacuum pump was removed and disassembled. The vanes and rotor remained intact. The composite vacuum drive was consumed by postimpact fire. ADDITIONAL INFORMATIONAirplane Flying Handb...

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA18FA016