N10GJ

Substantial
None

PIPER PA 28-180S/N: 287205192

Accident Details

Date
Wednesday, November 8, 2017
NTSB Number
CEN18LA036
Location
Carroll, OH
Event ID
20171122X13300
Coordinates
39.755554, -82.657218
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The total loss of engine power due to carburetor icing.

Aircraft Information

Registration
N10GJ
Make
PIPER
Serial Number
287205192
Engine Type
Turbo-shaft
Year Built
1972
Model / ICAO
PA 28-180M600
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
SALE REPORTED
Address
11202 W WINSLOW AVE
Status
Deregistered
City
TOLLESON
State / Zip Code
AZ 85353-9436
Country
United States

Analysis

On November 8, 2017, about 1230 eastern standard time, a Piper PA-28-180 airplane, N10GJ, was damaged during a forced landing following a loss of engine power near Carroll, Ohio. The pilot was not injured. The airplane received substantial damage to its left wing. The airplane was registered to and operated by the pilot under the provisions of Title 14 Code of Federal Regulations Part 91 as a personal flight. Visual meteorological conditions prevailed for the flight, which was not on a flight plan. The local flight originated from the Fairfield County Airport(LHQ), Lancaster, Ohio, about 1200.

The pilot reported that he was performing takeoff and landing practice and while on the downwind leg of the airport traffic pattern he applied carburetor heat, 10° flaps, turned on the fuel pump, and reduced throttle to 1,500 rpm to set up for the base leg. He stated that the engine suddenly stopped producing power and was unresponsive to throttle input. He attempted to restart the engine without success. He turned the airplane onto a base leg but had insufficient altitude to make it back to the airport and landed in a field.

Subsequent examination of the airplane revealed that it had about 36 gallons of fuel remaining. A ground run of the engine was performed and the engine started and was run for several minutes at power setting from 1,500 to 1,700 rpm. Additional testing of the airplane's electric fuel boost pump and engine driven fuel pump revealed that both pumps were capable of pumping fuel. No anomalies were discovered that would explain the loss of engine power.

The temperature and dew point recorded at the accident airport about the time of the accident were 9° and 2° Celsius respectively. The recorded temperature and dew point were in the range of susceptibility for serious carburetor icing at any power setting. An article on carburetor icing published by Flight Safety Australia stated that if ice forms in the carburetor of a fixed pitch propeller aircraft, the restriction to the induction airflow will reduce power and force a drop in rpm, which might be accompanied or followed by rough running as the fuel/air mixture ratio is upset. Applying carburetor heat introduces less dense hot air which will cause a further drop in rpm.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN18LA036