N353RA

Substantial
None

S.O.C.A.T.A. MS893ES/N: 13180

Accident Details

Date
Thursday, January 11, 2018
NTSB Number
CEN18LA073
Location
Wadsworth, OH
Event ID
20180111X55713
Coordinates
41.003055, -81.756385
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The pilot’s failure to apply carburetor heat during the approach, which resulted in a loss of engine power due to carburetor icing.

Aircraft Information

Registration
N353RA
Make
S.O.C.A.T.A.
Serial Number
13180
Year Built
1978
Model / ICAO
MS893E

Registered Owner (Historical)

Name
KEENE ROGER D
Address
4149 BEAT RD
Status
Deregistered
City
LITCHFIELD
State / Zip Code
OH 44253-9753
Country
United States

Analysis

On January 11, 2018, about 1130 eastern standard time, a S.O.C.A.T.A. MS893E airplane, N353RA, was substantially damaged during a forced landing at Wadsworth Municipal Airport (3G3), Wadsworth, Ohio. The private pilot was not injured. The airplane was registered to and operated by the pilot under the provisions of Title 14 Code of Federal Regulations Part 91 as a ferry flight. Day visual meteorological conditions prevailed for the flight, which departed without a flight plan from Reader-Botsford Airport (67D), Wellington, Ohio, about 1120.

The pilot stated that the purpose of the flight was to ferry the airplane, which had an expired annual inspection, to a new hangar. During the approach to 3G3, the pilot noticed a loss of engine power. Following unsuccessful attempts to restore engine power, the pilot executed a forced landing, during which the airplane impacted trees and damaged both wings.

Examination of the airplane at the accident site revealed the carburetor heat control was in the off position. The left fuel tank contained nine gallons of fuel and the right fuel tank contained seven gallons of fuel. The fuel contained no contaminants and no obstructions were found in the fuel lines. The engine was rotated by hand utilizing the propeller and compression was observed at all cylinders, with normal valve train and crankshaft continuity. Both magnetos were rotated by hand and produced spark at all leads. The engine fuel pump was actuated and exhibited normal suction and compression of fuel. The carburetor filter was free of contaminants and no anomalies were noted with the carburetor. Examination of the engine and fuel system revealed no preimpact anomalies that would have precluded operation of the engine.

The pilot stated that although his normal habit pattern was to activate the carburetor heat control while on downwind, this action may not have occurred on the accident flight and he thought the power loss might have been caused by carburetor icing. He had not flown the airplane for more than a year.

The recorded temperature and dew point data from a nearby weather station were plotted on a carburetor icing chart. The charted data showed that the weather was conducive to serious icing at descent power near the time of the engine power loss.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN18LA073