N317KD

Substantial
None

DAYTON A DABBS MAGNI M-16S/N: 16169634

Accident Details

Date
Saturday, January 13, 2018
NTSB Number
CEN18LA079
Location
Point Venture, TX
Event ID
20180118X12003
Coordinates
30.379999, -98.011108
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The loss of engine power for reasons that could not be determined because a postaccident engine test run showed no anomalies that would have precluded normal operation, and the pilot's decision to conduct the flight at a low altitude.

Aircraft Information

Registration
Make
DAYTON A DABBS
Serial Number
16169634
Engine Type
Reciprocating
Year Built
2016
Model / ICAO
MAGNI M-16
Aircraft Type
Gyroplane
No. of Engines
1
Seats
2
FAA Model
MAGNI M-16

Registered Owner (Current)

Name
SILVA RONALD C
Address
11364 VOLCANO CT
City
GOLD RIVER
State / Zip Code
CA 95670-7218
Country
United States

Analysis

On January 13, 2018, about 1200 central standard time, an experimental amateur-built Magni M-16 gyroplane, N317KD, sustained substantial damage during a forced landing following a complete loss of engine power while maneuvering near Point Venture, Texas. The private pilot was not injured. The gyroplane's tail boom, rotor mast support, landing gear, and fuselage sustained damage during the forced landing. The aircraft was registered to Off The Ground, LLC and operated by the pilot under the provisions of Title 14 Code of Federal Regulations Part 91 as a personal flight. Visual meteorological conditions prevailed for the flight, which was not operated on a flight plan. The local flight originated from Taylor Municipal Airport (T74), Taylor, Texas about 0900.

The pilot reported that flight was a pleasure flight around a nearby lake with an intended return to the departure airport. He stated that he decreased altitude to fly over the shoreline by reducing power. Upon reaching 50 feet agl., he applied power to gain altitude, but the engine did not respond. He said that the gyroplane went into a stall and impacted the ground. In his report, the pilot noted that he should have maintained a higher altitude which would have allowed him to land safely by maintaining airspeed with the nose of the gyroplane down. He noted that he did not have time to regain airspeed due to the low altitude.

The gyroplane was examined after the accident by a Federal Aviation Administration (FAA) Inspector. During the examination, an engine test run was performed and the engine started and ran without any issues detected. The gyroplane's engine monitor was downloaded and the data for the accident flight showed that the engine rpm dropped from about 5,000 rpm to 1,000 rpm prior to the end of the collected data. The collected data contained only the following parameters: exhaust gas temperatures for each cylinder, water temperature, oil temperature, atmospheric pressure and rpm.

The temperature and dew point recorded at the Austin-Bergstrom International Airport, about 20 nautical miles southeast of the accident site were 7 degrees Celsius, and -7 degrees Celsius respectively. According to a carburetor icing probability chart contained in FAA Special Airworthiness Information Bulletin (SAIB) CE-09-35, entitled "Carburetor Icing Prevention", the recorded temperature and dew point were not in the range of susceptibility for carburetor icing.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN18LA079