N8401V

Substantial
Minor

AERO COMMANDER CALLAIR A 9S/N: 1601

Accident Details

Date
Saturday, February 24, 2018
NTSB Number
ERA18LA087
Location
Bunn, NC
Event ID
20180226X10119
Coordinates
35.926666, -78.248054
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
1
Uninjured
0
Total Aboard
1

Probable Cause and Findings

The glider instructor's delayed remedial action when the glider became out of position during aerotow, which resulted in excessive side-loading of the release hook and a delay in the glider's release from tow, which resulted in the towplane’s descent and impact with trees.

Aircraft Information

Registration
Make
AERO COMMANDER
Serial Number
1601
Engine Type
Reciprocating
Year Built
1970
Model / ICAO
CALLAIR A 9L29
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
1
FAA Model
CALLAIR A-9

Registered Owner (Current)

Name
GLENN LARRY W
Address
PO BOX 247
City
BUNN
State / Zip Code
NC 27508-0247
Country
United States

Analysis

On February 24, 2018, about 1230 eastern standard time, an Aero Commander Callair A-9 (Callair A-9), N8401V, was substantially damaged when it was involved in an accident near Bunn, North Carolina. The commercial pilot sustained a minor injury. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 glider tow flight.

The flight instructor of the Schweizer SGS-2-33A glider (N1186S) being towed aloft reported that 2 previous flights earlier that day, the student was demonstrating good progress in controlling the glider off tow and showing beginning competency on tow but occasionally required his corrections, which improved on the 2nd flight. The student executed the 3rd takeoff under control and when above the treeline with moderate turbulence which was similar to the conditions during the first 2 flights, a gust occurred. The glider moved down and to the right relative to the tow airplane with resulting slight amount of slack in the tow line. The student made appropriate control inputs to move the glider up and to the left, but the glider continued up and to the left at, "an alarming rate, reminding me of a winch launch, and we zoomed up to a maximum of what [he estimated] as [about] 400 ft [above ground level]", placing the glider in "…extremely out of position." About that time he took over the controls and made large forward and right stick movements, in addition to deploying full spoilers. Because the situation was not improving he determined they needed to release immediately and pulled twice with more force than usually required, then when the glider did not release which he later attributed to the side loads, he looked to confirm he was pulling the correct control and on the 3rd attempt yanked as hard as he could and the tow line released. He maneuvered the glider for an uneventful downwind landing.

The pilot of the Callair A-9 reported that the moment the glider became airborne, "it was a very turbulent tow" with the glider moving erratically back and forth. The flight continued and when he looked into the mirror, the glider was out of position, and he noted slack in the towline. The tow line slack went out causing the nose of the airplane to jerk about 35° to the left, which reduced the airspeed considerably. The glider continued to climb, causing the tow plane to be in a nose-low attitude. About that time, he attempted to release the glider, but because of the position of the tow release handle in the cockpit, he had difficulty reaching it. He eventually was able to reach the handle, but the glider released a split second before he could initiate the release. When the glider was released, the airplane was about 75 feet agl, or about 25 to 45 feet above the tree tops. The left wing then impacted trees, and the airplane then impacted the ground nearly fully inverted. The pilot reported no preimpact mechanical failure or malfunction.

Postaccident examination of the Callair A-9 by a Federal Aviation Administration inspector revealed the elevator control cable tensions were near zero and the rigging of the elevator was off related to the position relative to the horizontal stabilizer and the control stick in the cockpit. Examination of the Callair A-9 and Schweizer glider by a mechanic revealed the tow release of the Callair A-9 was within limits, while the tow release of the glider was above the maintenance manual limits; the amount was not specified.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA18LA087