N442AG

Substantial
None

LYNN PERRY CAVALONS/N: V00311

Accident Details

Date
Monday, March 26, 2018
NTSB Number
GAA18CA179
Location
Haverhill, NH
Event ID
20180326X21650
Coordinates
44.080001, -72.007774
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The pilot's failure to maintain directional control during a rejected takeoff. Contributing to the accident was the binding of the control stick, for an undetermined reason, which precipitated the rejected takeoff.

Aircraft Information

Registration
Make
LYNN PERRY
Serial Number
V00311
Engine Type
4-cycle
Year Built
2017
Model / ICAO
CAVALONBPAT
Aircraft Type
Rotorcraft
No. of Engines
1
Seats
2
FAA Model
CAVALON

Registered Owner (Current)

Name
COGLEY WILLIAM S
Address
398 DOUGLAS RD
City
WHITINSVILLE
State / Zip Code
MA 01588-2025
Country
United States

Analysis

The pilot of the gyroplane reported that, during the takeoff roll, after the front landing gear became light, he attempted to push the control stick forward, but was unable. He then used both hands in an attempt to push the stick forward. He realized he could not move the control stick forward and therefore could not control the gyroplane. He rejected the takeoff by reducing power, the gyroplane veered to the left, and the rotor struck the runway. Subsequently, the gyroplane rolled onto its left side, skidded down the runway, exited the left side of the runway, and impacted a snowbank.

The gyroplane sustained substantial damage to the rotor system and fuselage.

The pilot reported that he removed the rotor blade by removing the center pivoting bolt, and in doing so, the rotor head moved forward and freed the stick.

The Federal Aviation Administration sent two inspectors to examine the gyroplane. During the visit, the rotor head moved freely in all directions with no evidence of binding or restriction, and no discrepancies were noted with the torque tube or cabling in the keel tube. The brake and trim controls were also moved in various sequences and control positions, but there were no discrepancies found. The FAA inspector added that, with an inadvertent and or unnoticed activation of full aft trim prior to beginning the takeoff roll, there could be enough resistance created to generate the conditions the pilot experienced.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# GAA18CA179