N9456P

Destroyed
Fatal

PIPER PA 24-260S/N: 24-4964

Accident Details

Date
Tuesday, April 10, 2018
NTSB Number
WPR18FA119
Location
Scottsdale, AZ
Event ID
20180410X32846
Coordinates
33.635555, -111.897781
Aircraft Damage
Destroyed
Highest Injury
Fatal
Fatalities
6
Serious Injuries
0
Minor Injuries
0
Uninjured
0
Total Aboard
6

Probable Cause and Findings

The flight instructor's failure to maintain airplane control during the initial climb as a result of the airplane being loaded above its maximum gross weight and beyond its aft center of gravity limits. Contributing to the accident was a degraded engine power output due to a preexisting engine cylinder intake valve spring failure, which further reduced the airplane's climb capability.

Aircraft Information

Registration
N9456P
Make
PIPER
Serial Number
24-4964
Engine Type
Turbo-shaft
Year Built
1970
Model / ICAO
PA 24-260M600
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
REGISTRATION PENDING
Address
5901 N GRAND CANYON DR
Status
Deregistered
City
LAS VEGAS
State / Zip Code
NV 89149-1405
Country
United States

Analysis

HISTORY OF FLIGHT

On April 9, 2018, about 2048 mountain standard time, a Piper PA-24-260 airplane, N9456P, was destroyed when it impacted terrain shortly after takeoff from Scottsdale Airport (SDL), Scottsdale, Arizona. The airline transport pilot, the student pilot, and four passengers were fatally injured. The airplane was registered to N9456P LLC and was operated by the pilots as a Title 14 Code of Federal Regulations Part 91 personal flight. Nighttime visual meteorological conditions prevailed, and no flight plan was filed for the cross-country flight, which was destined for North Las Vegas Airport (VGT), Las Vegas, Nevada.

Earlier that evening, the airline transport pilot flew the airplane from VGT to SDL to pick up the student pilot and the passengers and fly them to VGT. The inbound flight, which was the airline transport pilot's first flight in the airplane, departed from VGT at 1842 mst and landed at SDL at 2018.

A video surveillance camera at SDL located on the ramp where the airplane was parked captured the occupants as they began to board the airplane about 2028. The surveillance video, along with photographs and videos posted to social media by one of the occupants, revealed that the student pilot occupied the front left seat and that the airline transport pilot occupied the front right seat.

A video surveillance camera located midfield on the west side of the runway captured the airplane's departure from runway 03. The video showed that the airplane's wings were rocking during and shortly after rotation.

The tower controller reported that, as the airplane began the departure roll, the lights on the wings were alternating up and down as if the pilot was rocking the wings. The controller also reported that, as the airplane passed the tower, the wings appeared to be stable but that the engine sounded as if it was not producing enough power. At that time, the controller asked the pilot if the airplane was experiencing any difficulty. According to the controller, the pilot responded, "we're good. We're just in training mode." The controller observed the airplane continue straight out but noted that it did not appear to be climbing. Over the departure end of the runway, the airplane made a left turn. A review of radar data revealed that the airplane's last depicted altitude, between 2046:18 and 2046:28, was about 200 ft above ground level, which occurred during the left turn. As the airplane continued in the left turn, the controller observed the airplane enter a nose-down attitude.

A traffic camera located about 0.5-mile northwest of the end of the departure runway recorded the airplane in a left bank. The bank angle continued to increase as the airplane descended, and its wings were nearly vertical. The camera then depicted the airplane's impact with terrain and a fireball.

Video captured by the traffic camera and the airport tower camera were used to estimate the trajectory and speed of the airplane. The airplane's ground speed was estimated at 75 ± 4 knots shortly after takeoff, and its climb rate was 270 ft per minute (fpm). Twelve seconds later, as the airplane entered the left turn near the end of the runway, its ground speed decayed to 50 ± 4 knots. The airplane began to descend and impacted the ground several seconds later. The airplane was airborne for about 70 seconds.

A witness located near the departure end of the runway was listening to the tower frequency and overheard the controller asking the pilot if the airplane was experiencing any difficulties. The witness looked down the runway and observed the airplane proceeding toward him. As the airplane flew by, the witness noted that the airplane appeared to drift toward the west side of the runway safety area while at low altitude and that the engine sounded as if it was not developing full power. The witness stated that the airplane, before reaching the end of the runway, started "an early left crosswind turn." The witness also stated that the airplane continued in the turn and started to descend just before disappearing from sight behind buildings and trees. Seconds later, the witness heard an explosion and saw a plume of smoke and fire.

Another witness located on the ramp observed the boarding process and watched the airplane taxi toward the runway. The witness lost sight of the airplane but was able to hear what sounded like a typical preflight engine run-up. The witness then observed the airplane accelerate down the runway and stated that, about midway, the wings began to roll in an "extreme" motion. The witness reported that the oscillations eventually diminished, and that the airplane began to climb, reaching an altitude that was about level with the top of the adjacent airport buildings. The airplane continued at an altitude that was about the same altitude and then began a climbing left turn, which appeared similar but lower than most aircraft departing the traffic pattern. As the turn progressed, the airplane's attitude changed to pitch down, and the airplane disappeared from sight. A fireball ensued. The witness did not hear any unusual sounds or see the airplane emitting smoke, fire, or vapors, and she stated that the engine sounded similar to the airplanes that she observes.

PERSONNEL INFORMATION

The pilot held an airline transport pilot certificate with airplane single-engine land and multiengine land ratings. He also held a flight instructor certificate with ratings for airplane single engine, airplane multiengine, and instrument airplane. On February 7, 2018, the pilot received a special issuance first-class medical certificate with the following limitation: "Not valid for any class after 08/31/2018." At the time of his most recent medical application, the pilot reported that he had 5,200 hours of total flight experience, 500 hours of which were in the previous 6 months. The pilot's employer reported that, from August 24, 2017 (his start date with the company), to April 8, 2018 (the day before the accident), the pilot had accumulated 161 hours of flight time, 69 hours of which were in 2018. The pilot had accumulated about 2 hours of flight time in the accident airplane.

The student pilot had been receiving lessons from another flight instructor. He did not possess a student pilot or airman medical certificate. The student pilot's total flight experience could not be determined.

AIRCRAFT INFORMATION

The single-engine, retractable gear airplane was manufactured in 1970 and was powered by a 260-horsepower, 6-cylinder, fuel-injected Lycoming IO-540-N1A5 engine and a two-blade constant-speed Hartzell propeller. The airplane was equipped with six seats.

The last entry in the airframe logbook indicated that the airplane received an annual inspection on December 1, 2017, at a total airframe time of 6,158 hours.

According to a logbook entry dated August 1, 1973, the airplane's empty weight was 2,007 pounds, the useful load was 1,193 pounds, and the empty weight center of gravity (CG) was 87.22 inches. No additional weight and balance data were located. The airplane flight manual listed a maximum allowable gross weight of 3,200 pounds and a CG range between 80.5 and 93.0 inches aft of datum.

The last obtained fuel receipt was dated April 3, 2018, from VGT. A search of commercially available flight software indicated that the flight from VGT to SDL on the day of the accident was the first flight after the last refueling.

The combined weight of the pilot and the student pilot was about 375 pounds, the combined weight of the two passengers (a male and female) located in the middle row was about 320 pounds, and the combined weight of the two passengers (both female) in the aft row was about 252 pounds. All of the estimated weights included 15 pounds of carry-on baggage per person. An estimated fuel load of 63.44 gallons was calculated based on the maximum usable fuel (86 gallons) subtracted by the fuel burned during the flight from VGT to SDL (22.56 gallons based on an in-flight power setting of 75%).

Given the passenger weights along with the estimated fuel at the time of initial taxi, the airplane would have weighed about 3,335 pounds at the time of takeoff, and its CG would have been 95.22 inches aft of datum. These values were 135 pounds above the airplane's maximum gross weight and 2.22 inches aft of the CG.

With a calculated density altitude of 3,300 ft (based on meteorological conditions about the time of the accident), an airplane weight of 3,200 pounds, flaps at 15°, and the landing gear extended, the expected rate of climb is 700 fpm. When the airplane is in a clean configuration with the same weight and density altitude, the expected rate of climb is 1,110 fpm.

METEOROLOGICAL INFORMATION

The 1953 SDL weather observation included wind from 160° at 3 knots, visibility 10 miles, clear skies, temperature 28°C, dew point -5°C, and altimeter setting 29.94 inches of mercury. Based on these values, the calculated density altitude was about 3,300 ft.

WRECKAGE AND IMPACT INFORMATION

The airplane came to rest in a golf course about 1/4-mile northwest of the end of the runway 03

at an elevation of 1,484 ft. All major sections of the airplane were recovered at the accident site. The main wreckage sustained extensive impact and thermal damage and was contained within a debris field about 180 ft in length and 40 ft wide. The right wing, which remained partially attached to the fuselage, appeared to have struck a tree during the impact sequence. The left wing had fragmented into several sections and had separated from the fuselage. Both the left and right main landing gear had detached from their respective wings.

The empennage was intact and had separated from the aft fuselage due to thermal damage. The stabilator and rudder remained secured at their respective attach points. The rudder cables remained attached to the rudder horn. The stabilator cables remained attached to the stabilator horn tube. The stabila...

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# WPR18FA119