N3292Y

Substantial
Minor

CESSNA 182S/N: 18254292

Accident Details

Date
Monday, May 7, 2018
NTSB Number
CEN18LA162
Location
Broomfield, CO
Event ID
20180507X42518
Coordinates
39.908889, -105.117225
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
1
Uninjured
0
Total Aboard
1

Probable Cause and Findings

The overstress fracture of the upper link of the nose landing gear torque link assembly, which resulted in the pilot’s inability to maintain directional control during landing.

Aircraft Information

Registration
N3292Y
Make
CESSNA
Serial Number
18254292
Engine Type
Reciprocating
Year Built
1962
Model / ICAO
182C182
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
BURNELL ROGER J
Address
14855 W 58TH PL
Status
Deregistered
City
GOLDEN
State / Zip Code
CO 80403-1202
Country
United States

Analysis

On May 7, 2018, about 1139 mountain daylight time, a Cessna 182E airplane, N3292Y, was substantially damaged when it was involved in an accident near Broomfield, Colorado. The commercial pilot sustained minor injuries. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

The pilot departed and flew to his private grass airstrip, where he made two uneventful full-stop landings before returning to the departure airport. The pilot reported that he conducted a normal approach to runway 30L, and that the airplane initially touched down on the main landing gear, but when the nose landing gear contacted the runway, the airplane immediately swerved right and nosed over in the grass beside the runway.

A witness reported seeing the airplane on final approach to runway 30L with its nose wheel rotated about 75° from its normal alignment. The airplane initially touched down on its main landing gear; however, when the nose wheel contacted the runway, it did not realign with the runway heading; the airplane immediately swerved to the right. The nose landing gear separated from the airplane about 100 yards into the right swerve. The airplane subsequently departed the right runway edge and nosed over.

An onsite examination revealed that the vertical stabilizer, rudder, and right wing strut were substantially damaged. The nose landing gear torque link assembly had fractured, which allowed the nose wheel to rotate freely on the landing gear strut. The fractured scissor assembly and associated hardware were retained for additional examination at the National Transportation Safety Board (NTSB) Materials Laboratory in Washington D.C.

The NTSB laboratory examination of the torque link assembly revealed a fracture of the upper link arm near its upper end. The fracture exhibited features consistent with a downward bending overstress failure. The examination also identified an isolated area of preexisting fatigue on the right flange and a closed crack on the left flange, neither of which contributed to the bending overstress failure of the upper torque link.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN18LA162