Accident Details
Probable Cause and Findings
The pilot’s decision to take off with the airplane over its maximum gross weight due to his failure to perform preflight weight and balance calculations, which affected the airplane’s takeoff performance, and his subsequent decision to abort the takeoff with too little runway remaining, which resulted in a runway excursion.
Aircraft Information
Registered Owner (Current)
Analysis
The pilot reported that, before the flight, he performed weight and balance and performance calculations with the initial fuel level in the airplane. The airplane fuel tanks were then filled full of fuel, but he did not amend the weight and balance or performance calculations.
The pilot reported that, during takeoff, after the airplane became airborne, he did not feel comfortable with the way the airplane was performing, so he reduced power and landed the airplane on the remaining runway. He added that, he did not have enough runway to stop and attempted to exit on a taxiway, but "understeered" and the airplane exited the runway into a ditch.
The airplane sustained substantial damage to the fuselage.
The pilot reported on the National Transportation Safety Board 6120.1 Form that the airplane's maximum gross weight was 2,460 pounds and that the weight at the time of the accident was 2,600 pounds, about 140 pounds over the maximum gross weight.
The pilot reported that there were no preaccident mechanical failures or malfunctions with the airplane that would have precluded normal operation.
Data Source
Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# GAA18CA276