N9058F

Substantial
None

CESSNA 177S/N: 17700304

Accident Details

Date
Tuesday, May 15, 2018
NTSB Number
CEN18LA174
Location
Fort Wayne, IN
Event ID
20180516X20345
Coordinates
41.169998, -85.180000
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

The failure of the oil cooler due to a defect in the brazed joint, which resulted in a loss of engine power due to oil starvation.

Aircraft Information

Registration
N9058F
Make
CESSNA
Serial Number
17700304
Engine Type
Reciprocating
Year Built
1967
Model / ICAO
177C177
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
SALE REPORTED
Address
6000 DOUGLAS DR N
Status
Deregistered
City
CRYSTAL
State / Zip Code
MN 55429-2314
Country
United States

Analysis

On May 15, 2018, at 1455 eastern daylight time, a Cessna 177 airplane, N9058F, was substantially damaged during a forced landing near Fort Wayne, Indiana. The commercial pilot and passenger were not injured. The airplane was registered to and operated by the pilot under the provisions of Title 14 Code of Federal Regulations Part 91 as a personal flight. Visual meteorological conditions prevailed for the flight, which was operated on an instrument flight rules flight plan. The local flight originated from the Smith Field Airport (SMD), Fort Wayne, Indiana, at 1453.The pilot reported that shortly after takeoff as he leveled the airplane at 2,600 ft mean sea level, the engine rpm began decreasing and he heard a "thumping" noise in the engine. He lowered the nose of the airplane to maintain 80 mph and turned back toward the airport. The thumping noise increased, and he smelled burning oil just before the engine quit. The pilot selected a field for a forced landing and as he approached the field, he banked to the left to avoid overrunning the field. As he banked, the left wingtip contacted the ground and the airplane slid sideways collapsing the nose landing gear. Both wings sustained substantial damage.

According to the responding Federal Aviation Administration Inspector, an examination of the engine revealed no oil on the engine oil dip stick. Oil was visible on the right side of the cowling and oil was coming from the oil cooler. According to the maintenance records, the engine, including the oil cooler, was new and had been installed about 8 hours prior to the accident flight.

The oil cooler was sent to the National Transportation Safety Board Materials Laboratory in Washington, DC, for further examination. Examination of the oil cooler revealed that the leak came from between the plates forming the third oil circuit from the bottom. There was no evidence of mechanical damage from an external source and no evidence of bulging or other distortions.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN18LA174