N4323N

Substantial
Minor

AEROVODOCHODY L 29 DELFINS/N: 194145

Accident Details

Date
Friday, June 8, 2018
NTSB Number
CEN18LA218
Location
Moriarty, NM
Event ID
20180611X11608
Coordinates
34.982223, -105.990837
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
2
Uninjured
0
Total Aboard
2

Probable Cause and Findings

The pilot’s failure to maintain a proper glidepath during a visual approach and the flight instructor’s delayed remedial action, which resulted in ground impact before the runway.

Aircraft Information

Registration
N4323N
Make
AEROVODOCHODY
Serial Number
194145
Engine Type
Turbo-jet
Year Built
1971
Model / ICAO
L 29 DELFINL29
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
BENDER THOMAS G
Address
PO BOX 2031
Status
Deregistered
City
MORIARTY
State / Zip Code
NM 87035-2031
Country
United States

Analysis

On June 8, 2018, about 0753 mountain daylight time, an Aerovodochody L29 Deflin airplane, N4323N, was substantially damaged during a visual approach to Moriarty Airport (0E0), Moriarty, New Mexico. The pilot and flight instructor suffered minor injuries. The airplane was registered to and operated by the pilot under the provisions of 14 Code of Federal Regulations Part 91 as an instructional flight. Day visual meteorological conditions prevailed for the local flight, which departed about 0745 without a flight plan.

Following his recent purchase of the vintage, single-engine, turbine powered trainer airplane, the pilot was receiving his second training flight and accomplished a takeoff and traffic pattern for Runway 26. While on final approach, the flight instructor told the pilot to increase engine power after the airplane descended below glide path with a slow airspeed. After the engine did not respond as the flight instructor expected, he assumed control of the airplane and applied full power. The airplane continued to settle and impacted the ground about ½ mile short of the Runway 26 threshold, damaging both wings.

The flight instructor stated that he had "let his guard down" during the final approach and had not intervened quick enough as the airplane descended below the glide path. He was aware of the engine's "slow spool up" characteristic and viewed this issue, as well as the high-density altitude conditions, as contributors to his inability to counteract the airplane's sink rate after applying full power.

The pilot did not recall details of the final approach due to a concussion that he suffered during the accident. Although a previous military navigator, the pilot was not experienced piloting a turbine powered airplane. The flight instructor did not realize the pilot's military flight experience occurred as a navigator.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN18LA218