Summary
On July 10, 2018, a Robinson R44 (N144DJ) was involved in an incident near Rulo, NE. All 1 person aboard were uninjured. The aircraft sustained substantial damage.
The National Transportation Safety Board determined the probable cause of this incident to be: The pilot's improper collective application, which resulted in low rotor rpm during the takeoff climb and a subsequent ground collision. Contributing to the accident was the pilot’s self-induced pressure to complete the operation.
According to the helicopter pilot, he was performing a night agricultural flight. During takeoff from a platform located on top of the tender, his collective application was too aggressive, and during the ascent the engine sputtered. The engine RPM and main rotor RPM decreased, and he tried to regain the RPMs by lowering the collective.
The helicopter was moving forward and descending, so he applied aft cyclic to arrest the forward movement, and he attempted to land. The left skid touched down in the soft dirt and the pilot applied aft cyclic to prevent a nose over, but the main rotor blades struck the tailboom. The helicopter rolled forward, and the nose of the helicopter spun to the left before the helicopter came to rest on its left side.
This incident is documented in NTSB report GAA18CA408. AviatorDB cross-references NTSB investigation data with FAA registry records to provide comprehensive safety information for aircraft N144DJ.
Accident Details
Probable Cause and Findings
The pilot's improper collective application, which resulted in low rotor rpm during the takeoff climb and a subsequent ground collision. Contributing to the accident was the pilot’s self-induced pressure to complete the operation.
Aircraft Information
Registered Owner (Current)
Analysis
According to the helicopter pilot, he was performing a night agricultural flight. During takeoff from a platform located on top of the tender, his collective application was too aggressive, and during the ascent the engine sputtered. The engine RPM and main rotor RPM decreased, and he tried to regain the RPMs by lowering the collective.
The helicopter was moving forward and descending, so he applied aft cyclic to arrest the forward movement, and he attempted to land. The left skid touched down in the soft dirt and the pilot applied aft cyclic to prevent a nose over, but the main rotor blades struck the tailboom. The helicopter rolled forward, and the nose of the helicopter spun to the left before the helicopter came to rest on its left side.
The helicopter sustained substantial damage the fuselage, tail rotor drive system and skid tubes.
Additionally, the pilot asserted that the accident could have been prevented if he would not have been in a hurry to complete the operation.
The pilot reported that there were no mechanical malfunctions or failures with the helicopter that would have precluded normal operation.
Data Source
Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# GAA18CA408