N397AS

Substantial
Serious

Air Tractor AT802S/N: 802A-0563

Accident Details

Date
Tuesday, August 14, 2018
NTSB Number
WPR18LA222
Location
Northport, WA
Event ID
20180814X14134
Coordinates
48.980278, -118.017770
Aircraft Damage
Substantial
Highest Injury
Serious
Fatalities
0
Serious Injuries
1
Minor Injuries
0
Uninjured
0
Total Aboard
1

Probable Cause and Findings

A total loss of engine power during a climb due to an accumulation of molten environmental particles, the source of which could not be determined based on the available evidence, which resulted in a forced landing.

Aircraft Information

Registration
N397AS
Make
AIR TRACTOR
Serial Number
802A-0563
Engine Type
Turbo-shaft
Year Built
2014
Model / ICAO
AT802AT8T
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
WELLS FARGO TRUST CO NA TRUSTEE
Address
MAC: U1228-51
299 S MAIN ST FL 5
Status
Deregistered
City
SALT LAKE CITY
State / Zip Code
UT 84111-2689
Country
United States

Analysis

On August 14, 2018, about 1500 Pacific daylight time, an Air Tractor AT-802A, N397AS, was substantially damaged when it was involved in an accident near Northport, Washington. The pilot was seriously injured. The airplane was operated as a public use aircraft under the provisions of Title 14 Code of Federal Regulations Part 91.

According to the Washington State Department of Natural Resources, the airplane was operated under a call-when-needed contract as a single-engine air tanker.

The purpose of the flight was to support of firefighting operations in Colville National Forest, which is about 11 miles northwest of Northport. The accident airplane was one of three airplanes deployed to respond to the fire. The three airplanes had made four successful water drops and had just scooped water from the Columbia River for a fifth drop. The airplanes were climbing through an altitude of 4,600 ft mean sea level when two of the pilots heard the pilot of the accident airplane announce “mayday” and state that his airplane was losing engine power.

The pilot of the accident airplane stated that the engine was running nominally until he heard “a rather loud bang,” which was followed by a total loss of engine power. He stated that the compressor was running and was responsive to throttle inputs but that there was no noticeable thrust. The pilot was initially planning to land on an old logging road, but the landing area was too narrow and was lined with trees on both sides of the road. The pilot opted instead to stall the airplane to the treetops. After impact with the trees, the airplane came to rest upright at the base of the trees adjacent to the road.

A Federal Aviation Administration inspector responded to the accident site and reported that the entire airplane came to rest there. The inspector noted that the cowling and one wing were coated with oil and that the engine was damaged.

Examination of the accident site by the US Forest Service revealed that the airplane impacted trees adjacent to a fire road The fuselage came to rest upright on a magnetic heading of about 232° and at an elevation of 3,570 ft mean sea level. The first identified point of impact was a 50- to 75-ft tall tree that had damaged limbs near the top of the tree. The debris path was oriented on a magnetic heading of 143° and was about 345 ft in length. Various portions of airplane fragments were distributed throughout the debris path. Additionally, several trees were damaged along the debris path.

Postaccident examination of the engine revealed foreign melted debris in the engine combustion chamber with the molten mass stuck to the combustors, turbine vane rings, and turbine blades. The debris was identified as environmental particles, but the source of the debris was not identified.

A second-stage power turbine blade exhibited fatigue signatures. According to Pratt & Whitney Canada, the fatigue appeared to have initiated from several regions of “microshrinkage porosities.” Pratt & Whitney Canada also stated that there was no foreign melted debris on the fracture surface of the second-stage power turbine blade. The fracture faces of the first and second stage power turbine blades exhibited overload signatures.

Inspections and functional tests were performed on the fuel pump, fuel control unit, flow divider valve, fuel oil heat exchanger, overspeed governor, and fuel nozzles. Additionally, the compressor bleed valve and propeller governor were disassembled and inspected. No mechanical anomalies were found that would have precluded normal operation.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# WPR18LA222