N78JE

Substantial
None

CESSNA LC41S/N: 411030

Accident Details

Date
Monday, December 31, 2018
NTSB Number
ERA19LA081
Location
Apopka, FL
Event ID
20181231X83152
Coordinates
28.702777, -81.586669
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

A partial loss of engine power during a go-around for reasons that could not be determined based on the available information, which resulted in a forced landing.

Aircraft Information

Registration
Make
CESSNA
Serial Number
411030
Engine Type
Reciprocating
Year Built
2008
Model / ICAO
LC41C14T
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
4
FAA Model
LC41-550FG

Registered Owner (Current)

Name
DODSON INTERNATIONAL PARTS INC
Address
2155 VERMONT RD
City
RANTOUL
State / Zip Code
KS 66079-9014
Country
United States

Analysis

On December 30, 2018, about 2025 eastern standard time, a Cessna LC41-550FG, N78JE, was substantially damaged during a forced landing at Apopka Airport (X04), Apopka, Florida. The private pilot was not injured. The airplane was operated by Hardwood Transport LLC under the provisions of Title 14 Code of Federal Regulations Part 91. Night, visual meteorological conditions prevailed, and no flight plan was filed for the flight to X04. The flight departed Greater Binghamton Airport (BGM), Binghamton, New York about 1523.

The pilot reported that he left BGM with full fuel tanks, or 102 usable gallons of fuel on board. Following an uneventful flight, he set up for a visual approach to runway 33 at X04. While on final approach, he observed animals on the runway. He performed a go-around and noted that the engine did not produce full power when the throttle was advanced. While on the downwind leg of the traffic pattern, the airplane would not maintain altitude, so the pilot performed a forced landing. The airplane collided with trees and came to rest in a wooded area off the airport property.

The wreckage was recovered to a storage facility and was examined by investigators. Both fuel tanks were breached during the impact sequence and the tanks were dry. The wire bundle connecting the boost pump was observed separated. When reconnected, the wire bundle was tight. Blue, contaminant free fuel was observed in the fuel strainer bowl. The fuel caps were observed installed in the filler necks.

The engine was sent to the manufacturer's facility for examination. Due to the minor amount of impact damage to the engine, the investigation team elected to attempt a test run. After some minor repairs to ready the engine for the test cell, the engine experienced a normal start on the first attempt without hesitation or stumbling in observed RPM. Throughout the test phase, the engine accelerated normally without any hesitation, stumbling or interruption in power and demonstrated the ability to produce rated horsepower.

The airplane was equipped with a Garmin G1000 integrated flight deck. The G1000 recorded flight and systems data, including fuel quantity and engine performance. The data indicated that the flight began with 51 gallons per tank, or 102 gallons total useable fuel on board. Fuel quantity indications during the final 15 minutes were erratic; however, the total fuel quantity about 15 minutes prior to the accident was about 17 gallons. The average fuel flow during the same time period was about 13.3 gallons/hr.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA19LA081