N2021T

Destroyed
Fatal

Beech 36S/N: E-1325

Accident Details

Date
Thursday, January 17, 2019
NTSB Number
CEN19LA055
Location
Fredericksburg, TX
Event ID
20190118X92207
Coordinates
30.260555, -98.906944
Aircraft Damage
Destroyed
Highest Injury
Fatal
Fatalities
1
Serious Injuries
0
Minor Injuries
0
Uninjured
0
Total Aboard
1

Probable Cause and Findings

The loss of engine power due to fatigue failure of the crankshaft.

Aircraft Information

Registration
N2021T
Make
BEECH
Serial Number
E-1325
Engine Type
Reciprocating
Year Built
1978
Model / ICAO
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
BIG FUGA LLC
Address
43 TROPHY RDG
Status
Deregistered
City
SAN ANTONIO
State / Zip Code
TX 78258-7716
Country
United States

Analysis

On January 17, 2019, about 1650 central standard time, a Beech A-36 airplane, N2021T, was destroyed when it impacted terrain in Fredericksburg, Texas. The pilot was fatally injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

The airplane was flying from Bulverde Airpark, San Antonio, Texas, to Gillespie County Airport (T82), Fredericksburg, Texas, when another pilot reportedly heard a Bonanza (Beech A-36) pilot announce a "mayday" call on the common traffic advisory frequency, indicating the airplane's engine was on fire.

A review of aircraft records revealed the pilot had purchased the airplane in October 2018 and had flown the airplane on two flight that month for a flight time of 5.0 hours. The records noted that the engine was last overhauled on December 9, 2010, at a tachometer time of 1,585.1 hours and had accumulated 412.2 hours at the time of the October 2018 annual inspection.

The airplane was equipped with a Lycoming TIO-540 reciprocating engine and a Hartzell propeller under Supplemental Type Certificate SA762NW, Machen Inc. engine and propeller conversion.

The airplane's initial impact point was the edge of a field about 1 mile north of T82; the airplane then impacted a slightly elevated country road and came to rest upright. A post-crash fire consumed a majority of the airframe.

The airplane was initially recovered to an impound yard. After the government shutdown, the wreckage was then moved to aircraft salvage facility near Lancaster, Texas, where an examination was conducted by the National Transportation Safety Board (NTSB) Investigator-in-Charge (IIC), and technical representatives from the engine and airframe manufacturers.

A postaccident examination revealed that the engine exhibited fire damage. An attempt to manually rotate the engine was limited due to internal binding. Disassembly of the engine revealed a broken camshaft and crankshaft. The broken parts, along with the cylinders and pistons were sent to the NTSB Material Laboratory for examination. The laboratory noted crack arrest marks in the crankshaft, consistent with fatigue. The examination also noted that the fatigue initiated in the fillet radius at the forward end of the number 6 connecting rod journal. Multiple crack origins and prominent crack arrest lines were consistent with the relatively high stress associated with crack initiation.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN19LA055