N45MJ

Substantial
None

Piper PA31S/N: 31-7912104

Accident Details

Date
Friday, March 8, 2019
NTSB Number
ERA19LA125
Location
Leesburg, FL
Event ID
20190311X63755
Coordinates
28.822778, -81.808334
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

Maintenance personnel’s improper rigging of the main landing gear actuators, which resulted in the collapse of the right main landing gear.

Aircraft Information

Registration
Make
PIPER
Serial Number
31-7912104
Engine Type
Reciprocating
Model / ICAO
PA31PA31
Aircraft Type
Fixed Wing Multi Engine
No. of Engines
2
Seats
8
FAA Model
PA-31-325

Registered Owner (Current)

Name
FOLLOWELL ROBERT L
Address
9200 FOREST BEND CT
City
GERMANTOWN
State / Zip Code
TN 38138-8535
Country
United States

Analysis

On March 8, 2019, about 1000 eastern standard time, a Piper PA-31-325, N45MJ, was substantially damaged when it was involved in an accident near Leesburg, Florida. The pilot was not injured. The airplane was operated by the pilot as a flight test under the provisions of Title 14 Code of Federal Regulations Part 91.

According to the pilot, he delivered his airplane to a maintenance facility for an annual inspection. It was suggested by maintenance personnel that an inner landing gear door kit be installed (STC SA00555DE) during the annual inspection. After the door kit installation was completed, numerous test flights were conducted. During the landing gear extension, two green landing lights appeared as expected, but the third light (right main landing gear) was very slow to illuminate. Adjustments were made after each flight, and on the last flight while taxiing back to the ramp after landing the right landing gear collapsed.

Examination of the airplane by a Federal Aviation Administration inspector revealed buckling of the right inboard wing.

Post-accident extension and retraction test were performed using a hydraulic test unit. Both normal and emergency (hand pump) landing gear extension and retraction test were performed. During normal extension it was noted the landing gear locking time was approximately 25 seconds, which exceeded the manufacturer’s specified time limit; however, the hydraulic test fixture used did not have flow control, which could account for this anomaly. It was discovered when checking the actuator rigging that both left and right main landing gear actuators did not drive the main gears into a locked position. Slight hand pressure on the gear door (inboard force) would keep the main landing gear from locking as actuator piston travel was bottomed out. When the force was removed, the weight of the gear would lock the gear.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA19LA125