N5028P

Substantial
None

Piper PA 24S/N: 24-31

Accident Details

Date
Sunday, March 17, 2019
NTSB Number
WPR19LA098
Location
Reno, NV
Event ID
20190319X93150
Coordinates
39.669998, -119.879997
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
3
Total Aboard
3

Probable Cause and Findings

Failure of the engine mount due to internal corrosion and wall thinning, which resulted in a loss of directional control and nose gear collapse during landing.

Aircraft Information

Registration
N5028P
Make
PIPER
Serial Number
24-31
Engine Type
Turbo-shaft
Year Built
1958
Model / ICAO
PA 24M600
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
KOEHL DENNIS
Address
1310 LANDERWOOD DR
Status
Deregistered
City
RENO
State / Zip Code
NV 89511-1400
Country
United States

Analysis

On March 17, 2019, about 0810 Pacific daylight time, a Piper PA-24 airplane, N5028P, was substantially damaged when it was involved in an accident near Reno, Nevada. The private pilot and two passengers were not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

The pilot extended the landing gear shortly after entering the traffic pattern for landing and observed a green indication, which confirmed that the landing gear was down and locked. The airplane touched down normally on the main landing gear, but after the nose landing gear contacted the runway surface, the airplane veered to the left. The pilot stated that he corrected the airplane's direction, but the airplane then began to veer right of the runway centerline. He used the airplane's hand brake to decelerate while he attempted to return the airplane to the runway centerline, and the airplane veered to the left again and departed the left runway edge. The left wing impacted a runway distance remaining sign and the airplane spun to the left. As the airplane began to slide on its right side in gravel, the nose landing gear and right main landing gear collapsed before the airplane came to rest near the edge of a taxiway.

The airplane sustained substantial damage to the left wing and the stabilator. Additionally, the engine mount, which attached to the nose landing gear, had fractured.

According to logbook records, the airplane's most recent annual inspection was completed on October 23, 2018, at a total time of 3,563 flight hours. The preceding annual inspection was performed on March 3, 2011, at which time the airplane had accrued 3,545 flight hours. The airplane had accumulated about 15 total flight hours since its most recent inspection. According to the most recent annual inspection logbook entry, a gear retraction test was performed, and the gear warning horn was replaced. The mechanic who performed this service did not indicate if additional segments of the landing gear system were inspected.

The mechanic who recently serviced the accident airplane reported that his father had owned the airplane since the 1980s. After 1991, the airplane was parked, likely outside, until 2010, when it received an annual inspection and completed a round-trip flight to Los Angeles, California. The airplane was then parked outside and did not fly again until October 2018 when the accident pilot purchased it.

The engine mount connected both the nose landing gear and engine to the firewall, and the nose landing gear was connected to the engine mount through the oleo strut housing. Most of the nose landing gear assembly was intact with the exception of the left engine mount tubes, which were fractured. The tubes are represented in Figure 1 as 1, 2, 3, and 4 (the trunnion). According to a representative of the airplane manufacturer, this engine mount supported the nose landing gear.

A visual inspection of the nose landing gear assembly showed that the nose bell crank and nosewheel steering rods were intact. Additionally, the shimmy dampener displayed a slight bend, but still provided resistance when actuated by hand.

Figure 1: Nose Landing Gear Engine Mount Tubes and Trunnion

Portions of the engine mount were submitted to the NTSB Materials Laboratory for analysis. Each engine mount fracture surface was non-planar and rough, consistent with overstress. Moderate to heavy corrosion products were observed on the inner surfaces of each tube and several tubes displayed evidence of wall thinning from the internal corrosion. The exact order that the tubes failed could not be determined.

Figure 2: Location of Mount Fractures on NLG Assembly

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# WPR19LA098