N7622M

Substantial
None

Cessna 175S/N: 55922

Accident Details

Date
Thursday, April 4, 2019
NTSB Number
ERA19LA143
Location
Edgefield, SC
Event ID
20190404X74451
Coordinates
33.768890, -81.986663
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

The total loss of engine power due to a stuck engine exhaust valve. Contributing to the loss of engine power was the pilot’s failure to properly address the recurring stuck exhaust valve issue.

Aircraft Information

Registration
N7622M
Make
CESSNA
Serial Number
55922
Engine Type
Reciprocating
Model / ICAO
175C175
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
KINGDOM AIR CORPS
Address
39911 N GLENN HWY
Status
Deregistered
City
SUTTON
State / Zip Code
AK 99674-8005
Country
United States

Analysis

On April 4, 2019, about 1215 eastern daylight time, a Cessna 175, N7622M was substantially damaged when it was involved in an accident near Edgefield, South Carolina. The pilot and pilot-rated passenger were not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

The airplane had not been flown for about 6 years before being purchased about a week before the accident. The individual who inspected it for purchase noted a stuck valve during his examination of the engine and also during an engine run. After purchase, the wings were removed and the airplane was transported to an airport for reassembly. The pilot, who was also an airframe and powerplant mechanic, reinstalled the wings and performed an annual inspection the day before the accident. The pilot performed the annual inspection from memory without a checklist. During the inspection the pilot noted low compression in the No.2 cylinder, which he attributed to a stuck exhaust valve. He did not conduct a differential cylinder compression test. The corrective action consisted of staking the valve. Afterwards the engine was operated with no discrepancies noted. He then flew the airplane about 1 hour during 2 separate flights with no reported discrepancies.

The pilot stated that during the engine run-up check for the accident flight, the No. 2 cylinder exhaust valve stuck again. He secured the engine, staked the valve, and performed another engine run-up with no discrepancies noted. He performed an engine run-up before departure noting each magneto drop was about 150 rpm. He also performed several full throttle static engine runs noting that the maximum rpm attained was between 2,500 and 2,600 rpm. He then departed and after about 20 minutes of level flight the engine began to run "a little shaky" like there was a stuck valve. The pilot turned towards a nearby airport but the engine began to run rougher then lost power completely He spotted a field and set up for a forced landing. During the landing roll, while maneuvering to avoid livestock, the left wing collided with a power pole.

Postaccident examination of the airplane was performed by several Federal Aviation Administration (FAA) inspectors. An initial inspection revealed no contaminants of either fuel tank or fuel strainer; the airplane had about 25 gallons of fuel on-board. The carburetor bowl contained an unquantified amount of fuel, and the fuel strainer was full of uncontaminated fuel. There was no blockage from either tank through the fuel selector to the engine on any of the positions of the fuel selector valve. The air induction and exhaust systems were free of obstructions. Two ignition leads for the right magneto were noted to be swapped. The engine was started and operated to only 1,500 rpm due to safety concerns.

During operation of the engine there was a "noticeable skip coming from the engine." A check of the magnetos at low engine rpm revealed the engine "backfired and sputtered bad before shutting down" when the left magneto was selected, but the engine continued to run when the right magneto was selected. The inspectors did not have tools to determine the magneto-to-engine timing, or internal timing of the left magneto, which was removed and examined. It was disassembled completely in the field except for removing the coil and contactor and internally appeared to be in good condition. No further examinations of the left magneto were conducted, and the reason the engine lost power when it was selected was not determined.

The pilot later stated that following recovery of the airplane, he examined the engine and found the exhaust valve guide of one cylinder came out of the cylinder and attached to the valve. He also indicated that, on another cylinder, he found the pushrod socket out of position. The pilot did not respond to requests to clarify which two cylinders were affected.

According to Continental Aerospace Technologies Standard Practices Manual, cylinder removal and inspection is specified if one or more of the valves in the valve train are sticking.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA19LA143