N269P

Substantial
None

Schweizer 269CS/N: S1328

Accident Details

Date
Friday, May 24, 2019
NTSB Number
GAA19CA284
Location
Riverside, CA
Event ID
20190528X83837
Coordinates
33.951946, -117.444999
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
1
Total Aboard
1

Probable Cause and Findings

The student pilot's failure to maintain yaw control and the engine's rpm during transition to a hover, which resulted in hard landing.

Aircraft Information

Registration
N269P
Make
SCHWEIZER
Serial Number
S1328
Engine Type
Reciprocating
Year Built
1988
Model / ICAO
269CH269
Aircraft Type
Rotorcraft
No. of Engines
1

Registered Owner (Historical)

Name
INGOMA AERO INC
Address
1410 INDUSTRIAL DR
Status
Deregistered
City
ROYSE CITY
State / Zip Code
TX 75189-5410
Country
United States

Analysis

The student helicopter pilot reported that she had been working on her private helicopter pilot certificate over an extended period of time.

The student reported that the helicopter's throttle governor had been operational during previous solo flights, but it had failed months prior to the accident flight. She confirmed that she had flown the helicopter several times without the use of the governor, under the supervision of the instructor.

The day of the accident, she had flown three takeoffs and landings in the pattern with the flight instructor. After the third landing, the instructor exited the helicopter and authorized the student to perform her third solo flight.

The student reported that after accomplishing the before takeoff checks, the throttle was increased, and as she increased the collective pitch, she felt an "abnormal vibration," but she decided to continue with the flight. She increased the collective and applied left pedal, and the helicopter ascended, but the nose yawed rapidly to the left.

The student noted that the engine RPM increased, and she lowered the collective. The left skid contacted the ground hard, followed by the right skid, and the student decreased power, shut down the engine and exited the helicopter.

The helicopter sustained substantial damage to the aft skid tube cross-member.

The student pilot reported that several mechanical malfunctions existed with the helicopter during previous flights.

Examination of the helicopter and the operator's maintenance logbooks revealed that there were maintenance squawks that were incorrectly annotated, however, there were no mechanical malfunctions or failures that were observed during the examination that would have prevented normal helicopter operation.

The operator has implemented a policy to document and clear all future maintenance squawks associated with helicopters in their fleet.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# GAA19CA284