Accident Details
Probable Cause and Findings
A landing gear collapse following an undetermined loss of electrical power, which prevented the landing gear from fully extending.
Aircraft Information
Registered Owner (Current)
Analysis
On July 20, 2019, about 2345 Pacific daylight time, a Cessna R182 airplane, N3268C, was substantially damaged when it was involved in an accident near King City, California. The private pilot and passenger were not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.
According to the pilot, about 30 minutes into the flight in night conditions, the airplane's avionics started shutting down. He attempted to power them back up, but they shut down again after a short time. He then observed a discharge indication on the ammeter and advised air traffic control. The controller subsequently provided vectors to the nearest airport and another pilot on the frequency turned on the pilot-operated runway lighting at the airport.
During the approach for landing, the pilot lowered the landing gear lever to the down position and extended the wing flaps. The pilot stated he heard the landing gear extend and flaps deploy, and the airplane felt like it was in its normal landing configuration. He reported that, because he didn't want to lose sight of the runway, he elected not to use the emergency hand pump to ensure that the landing gear was down and locked. During the landing roll, the airplane felt “less maneuverable than normal” and came to a complete stop with the right wingtip and elevator contacting the runway.
The airplane came to rest on the right side of the runway. The nose landing gear was in the down and locked position. Neither of the main landing gear were fully extended. The right horizontal stabilizer and elevator sustained substantial damage.
Examination of the landing gear and electrical systems revealed no anomalies. The landing gear extended and retracted normally, and the emergency landing gear extension system operated normally. The alternator was removed from the airplane and was undamaged. The alternator was placed on a test bench and operated continuously until it reached its normal operating temperature. The alternator produced electrical power and no anomalies were noted.
Data Source
Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# WPR19LA201