N3469R

Destroyed
Fatal

Cessna 182S/N: 18258769

Accident Details

Date
Monday, August 5, 2019
NTSB Number
WPR19FA209
Location
Wolf Point, MT
Event ID
20190806X45857
Coordinates
48.435832, -105.760833
Aircraft Damage
Destroyed
Highest Injury
Fatal
Fatalities
2
Serious Injuries
0
Minor Injuries
0
Uninjured
0
Total Aboard
2

Probable Cause and Findings

The pilot's exceedance of the airplane's critical angle of attack while maneuvering to land, which resulted in an accelerated aerodynamic stall and subsequent loss of control.

Aircraft Information

Registration
N3469R
Make
CESSNA
Serial Number
18258769
Engine Type
Reciprocating
Year Built
1967
Model / ICAO
182C182
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
HEALD JAMES D
Address
PO BOX 74
Status
Deregistered
City
RECLUSE
State / Zip Code
WY 82725-0074
Country
United States

Analysis

HISTORY OF FLIGHTOn August 05, 2019, about 1445 mountain daylight time, a Cessna 182L, N3469R, was substantially damaged when it was involved in an accident near Wolf Point, Montana. The private pilot and passenger sustained fatal injuries. The airplane was operated as a Title 14 Code of Federal Regulations (CFR) Part 91 personal flight.

A witness stated that he owned the farm adjacent to the accident site. The pilot had built grain bins for him in the past and he had contracted him to build more. The pilot and passenger, an employee at the pilot’s company, planned to visit the farm that day. The pilot had discussed with the witness landing his airplane at the farm, and had been to the farm on previous occasions, but had never flown there.

The witness stated that the pilot called him at 1423 saying that he was flying over the town of Wolf Point and would be landing at the farm shortly. The witness, positioned near his grain bins, watched the airplane fly over his location and make a left turn to the west, paralleling the dirt road upon which he intended to land. The airplane then began a left turn to the east to come back and land. He observed the airplane make a sharp turn and descend into terrain. (refer to figure 1.) Upon impact, the airplane burst into flames and the witness drove his water truck to put out the fire.

Figure 1: Presumed Accident Flight Path (According to Witness)

PERSONNEL INFORMATIONA reconstruction of the pilot’s logbooks revealed that he had accrued about 16 hours of flight experience in the previous 3 months.

AIRCRAFT INFORMATIONThe pilot purchased the airplane in October 2017. On May 30, 2018, at an airframe total time of 3,191.41 hours, the airplane underwent major repairs to the wings after the pilot collided with a barn. Additionally, the left elevator was replaced, along with the aft bulkhead. The records indicated that the elevator and rudder control cables were adjusted to 30 lbs +/- 10 lbs. According to the logbooks, the only maintenance that occurred thereafter was an annual inspection in June 2019; about 100 flight hours after the repairs. There was no mention of the elevator or rudder in the entry for the June 2019 annual inspection. The tachometer at the accident site was destroyed and the airplane’s total time at the time of the accident could not be determined.

The Cessna Owner’s Manual stated that the stall characteristics were conventional, and an aural warning was provided by a stall warning horn, which sounded between 5 and 10 mph above the stall in all configurations. The Owner’s Manual indicated a stall speed of 64 mph at a gross weight of 2,800 lbs with flaps retracted. At bank angles of 30° and 60°, the stall speed increased to 69 and 91 mph, respectively. The maximum flap extension speed was 110 mph, and the recommended final approach speed was 75 knots.

AIRPORT INFORMATIONThe pilot purchased the airplane in October 2017. On May 30, 2018, at an airframe total time of 3,191.41 hours, the airplane underwent major repairs to the wings after the pilot collided with a barn. Additionally, the left elevator was replaced, along with the aft bulkhead. The records indicated that the elevator and rudder control cables were adjusted to 30 lbs +/- 10 lbs. According to the logbooks, the only maintenance that occurred thereafter was an annual inspection in June 2019; about 100 flight hours after the repairs. There was no mention of the elevator or rudder in the entry for the June 2019 annual inspection. The tachometer at the accident site was destroyed and the airplane’s total time at the time of the accident could not be determined.

The Cessna Owner’s Manual stated that the stall characteristics were conventional, and an aural warning was provided by a stall warning horn, which sounded between 5 and 10 mph above the stall in all configurations. The Owner’s Manual indicated a stall speed of 64 mph at a gross weight of 2,800 lbs with flaps retracted. At bank angles of 30° and 60°, the stall speed increased to 69 and 91 mph, respectively. The maximum flap extension speed was 110 mph, and the recommended final approach speed was 75 knots.

WRECKAGE AND IMPACT INFORMATIONThe accident site was located on a flat field composed of hard, dry dirt and short vegetation, about 21 nautical miles north of Wolf Point, Montana. The wreckage was found distributed over an approximate 40-foot distance with the nose pointed on a magnetic heading of about 340°. The main wreckage, consisting of all of the major control surfaces, was about 60 ft south of the road. The fuselage and inboard sections of the wings had been consumed by fire.

The first identified piece of debris was fragments of red lens, consistent with the tip of the left wing contacting the ground at the beginning of the accident sequence. Farther along the debris path, a disruption in the vegetation, similar in shape and size to that of a wing’s leading edge, contained pieces of lens consistent with the landing light. A crater in the dirt contained the two propeller blades.

During the postaccident examination, the engine was rotated via the vacuum pump drive. The engine’s internal mechanical continuity was established during rotation of the crankshaft and thumb compression was obtained on each cylinder. A borescope examination of all cylinders found no foreign object damage, no evidence of detonation, and no indication of excessive oil consumption. The top spark plugs were removed, and the electrodes were gray in color, which corresponded to normal operation according to the Champion Aviation Check-A-Plug AV-27 Chart.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# WPR19FA209