N8JR

Destroyed
Minor

Textron Aviation Inc 680AS/N: 680A0010

Accident Details

Date
Thursday, August 15, 2019
NTSB Number
ERA19FA248
Location
Elizabethton, TN
Event ID
20190815X74831
Coordinates
36.367221, -82.181663
Aircraft Damage
Destroyed
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
3
Uninjured
2
Total Aboard
5

Probable Cause and Findings

The pilot's continuation of an unstabilized approach despite recognizing associated cues and the flight crew's decision not to initiate a go-around before touchdown, which resulted in a bounced landing, a loss of airplane control, a landing gear collapse, and a runway excursion. Contributing to the accident was the pilot's failure to deploy the speedbrakes during the initial touchdown, which may have prevented the runway excursion, and the pilot's attempt to go around after deployment of the thrust reversers.

Aircraft Information

Registration
N8JR
Make
TEXTRON AVIATION INC
Serial Number
680A0010
Year Built
2015
Model / ICAO
680A

Registered Owner (Historical)

Name
JRM AIR LLC
Address
PO BOX 330
Status
Deregistered
City
MOORESVILLE
State / Zip Code
NC 28115-0330
Country
United States

Analysis

HISTORY OF FLIGHTOn August 15, 2019, about 1537 eastern daylight time, a Textron Aviation Inc. 680A, N8JR, was destroyed when it was involved in an accident near Elizabethton, Tennessee. The pilot and copilot were not injured and the three passengers sustained minor injuries. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 business flight.

In postaccident interviews and written statements, the pilot and copilot reported that the purpose of the flight was to drop off one of the three passengers at Elizabethton Municipal Airport (0A9), Elizabethton, Tennessee, before continuing the flight to San Antonio, Texas. The flight departed Statesville Regional Airport (SVH), Statesville, North Carolina, at 1519 and climbed to 12,500 ft mean sea level (msl). The preflight, departure, and en route portions of the flight were routine. Unless otherwise noted, the following sequence of events was derived from the download and review of data from onboard data and voice recording systems, and all speeds are indicated airspeed.

At 1527 (about 8 minutes after takeoff), the airplane began a descent from 12,500 ft msl to 5,400 ft msl; during the descent, the airplane turned right to varying headings between 325º and 342º. During this time, the flight crew discussed clouds in the area and the best ways to maneuver around them as well as traffic in the area and landmarks, including ridgelines, to help them identify 0A9. About 1530, the copilot announced via the airport's common traffic advisory frequency their intention to land on runway 24. At 1532:11, the pilot stated, "well it wouldn't hurt to slow down." About 33 seconds later, the descent resumed, and the airspeed decreased to 200 knots with the autothrottle engaged.

At 1533:00, the airplane began to turn left, and the crew conversation indicated that they had some difficulty visually acquiring the airport; the airplane then turned right and began to climb. At 1535:02, the descent resumed, and 10 seconds later the terrain avoidance and warning system (TAWS) excessive closure rate caution and warning alerts sounded in the cockpit as the airplane crossed a ridge at 710 ft above ground level (agl). The copilot asked the pilot if he saw the terrain, and the pilot responded, "yeah, I got it."

At 1535:27, the airplane began a shallow left turn to an extended final. As the approach to landing resumed, the descent rate increased; the autothrottle positioned the throttles to their minimum, 6º throttle lever angle, and the airspeed increased to 220 knots. At 1536:12, the pilot asked the copilot to position the flaps to the flaps 1 setting. The crew then manually positioned the throttles to 0º throttle lever angle, which disengaged the autothrottle; the throttles were not moved for the remainder of the approach. At 1536:29, the pilot stated, "slow down." At 1536:31, the pilot asked the copilot to lower the landing gear, and the copilot responded that he would after the airplane slowed down more. At 1536:36, the speedbrake lever was partially extended to a 33º lever angle, and the TAWS excessive descent rate caution alert sounded about 5 seconds later. (See figure 1 for the accident airplane's flight path until the first touchdown.) At 1536:47, about 3 nautical miles from touchdown and at 2,783 ft msl (781 ft agl), the speedbrake lever was extended to 41º for a total of 21 seconds then retracted after the airspeed decreased to 205 knots. At 1536:50, the landing gear were extended, and 7 seconds later, flaps 2 (15°) was selected; these actions were performed when the airplane reached the maximum speeds to perform those functions (205 knots and 195 knots, respectively).

Figure

1

: N8JR's approach, including speed and use of

speedbrakes

(in

yellow

), landing gear,

and flaps.

As the flaps were extending, the TAWS forward looking terrain alert rate of terrain closure caution alert sounded twice (at 1536:59 and at 1537:09), then a warning alert sounded (at 1537:11). The airplane was at an altitude of 2,159 ft msl (471 ft agl). Following these alerts, the copilot selected full flaps and the descent rate and airspeed decreased. At 1537:26, the copilot stated, "and I don't need to tell ya, we're really fast," and the pilot responded, "I'm at idle." Six seconds later, the pilot asked, "do I need to go around?" and the copilot responded, "no." At 1537:31, about 270 ft agl, the speedbrakes were partially extended for 5 seconds (to 140 ft agl). The pilot then stated, "I got the speed brakes out," to which the copilot responded, "well you should get rid of those because we don't wanna get a CAS [Crew Alerting System] m- or a thing sent to ya." Eight seconds before touchdown, at 1537:41, the pilot stated, "alright, I'll be on the T-Rs [thrust reversers] quickly." For the computed airplane weight, the reference speed (Vref) for the final approach was 108 knots; the airplane's airspeed at the runway's displaced threshold was 126 knots. Five seconds before touchdown, the airplane's descent rate was over 1,500 ft per minute (fpm).

According to airport surveillance video and recorded data, the airplane first briefly touched down with a bounce on the runway designator about 240 ft past the displaced threshold with about 3,860 ft of paved surface remaining. The airplane then touched down two more times, bouncing each time, then continued airborne over the runway until it touched down a fourth time with about 1,120 ft of paved surface remaining. See figure 2 for a depiction of the bounced landing detailing the landing gear touchdowns, vertical acceleration, and thrust reverser actions (the speedbrakes were not extended after touchdown, although the landing checklist indicated they should be).

Figure 2. Graph depicting the airplane's thrust reverser actions, landing gear touchdowns, and vertical acceleration (bold) during its bounced landing.

When the airplane touched down initially at 1537:49, it was travelling 126 knots (18 knots above Vref) and had a descent rate of 600 fpm (the maximum allowed per the airplane flight manual [AFM]). All three landing gear registered "on-ground" simultaneously with a vertical acceleration of 1.4 gravitational acceleration (g), and thrust reverser deployment was commanded 0.4 second after the landing gear first touched the ground as the throttles were moved to the reverse idle position; however, the airplane bounced after touching down for 0.6 second and was airborne again before the thrust reverser command could be executed.

When the airplane touched down a second time, 1.2 seconds later at 1.6 g, the nose landing gear touched down first, followed immediately by the right main landing gear. The left main landing gear never registered on-ground during the touchdown, and the airplane bounced and became airborne again after 0.4 second.

The airplane touched down a third time, 1.8 seconds later at 1.7 g and about 1,000 ft down the runway with about 3,100 ft of paved surface remaining. The thrust reversers unlocked 0.4 second after all three landing gear registered on-ground because the reverser deployment command from the first touchdown was still active. Almost immediately after the thrust reversers unlocked, the pilot advanced the throttles to idle, sending a thrust reverser stow command at 1537:54; however, the landing gear status changed to "in-air" almost simultaneously when the command was executed.

The airplane bounced after 0.6 second and became airborne a third time, and the in-air landing gear status triggered a cut in hydraulic power to the thrust reverser actuators, which is intended to prevent the airborne deployment of a thrust reverser. The cut in hydraulic power to the thrust reversers allowed the unlocked thrust reversers to be pulled open by aerodynamic forces. The amber "T/R UNLOCK CAS" message illuminated and the thrust reverser emergency stow switches began to flash. The pilot advanced the throttles to maximum takeoff power 0.7 second later in an attempt to go around; however, the thrust reversers reached full deployment 0.4 second after that. The airplane's full authority digital engine controls (FADEC), by design, prevented an increase in engine power while the thrust reversers were deployed. The red "T/R DEPLOY CAS" message was displayed in the cockpit, indicating that the thrust reversers were deployed, and the thrust reverser emergency stow switches continued to flash.

The pilots later reported that they attempted to conduct a go-around; however, the engines did not respond as expected, so they landed straight ahead on the runway. While the airplane was airborne, the crew partially retracted the flaps as the airspeed decreased from 119 knots to 91 knots. The pilot retarded the throttles partially but not to idle, then pushed the throttles forward again with no effect because the FADEC continued to prevent an increase in thrust; the pilot then pulled back the throttles to idle. While airborne for 9.6 seconds, the airplane reached an altitude of about 24 ft agl.

The stick shaker activated 0.5 second before the airplane touched down for the fourth and final time at 1538:03, warning of an imminent stall. The airplane touched down hard with a peak acceleration of 3.2 g on the left and right main landing gear, then the left main landing gear came off the ground then contacted the ground again. The nose gear contacted the ground about 0.5 second later. The left inboard wheel brake pressure increased to near maximum after the left main gear touched down; however, the left outboard and right wheel brake pressure did not increase significantly, indicating that only the left inboard tire was firmly contacting the runway. When all three landing gear touched down on the runway at 1538:06, the thrust reverser system was reenergized and the thrust reversers stowed 0.9 second later because the throttles were at idle.

Airport surveillance video showed that the right main landing gear collapsed at 1538:04 and ...

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA19FA248