Accident Details
Probable Cause and Findings
The total loss of engine power shortly after takeoff as a result of the private pilot’s failure to ensure the fuel selector was in the appropriate position and the certified flight instructor’s exceedance of the airplane’s critical angle of attack at the time of the engine power loss, which resulted in an aerodynamic stall and loss of airplane control.
Aircraft Information
Registered Owner (Current)
Analysis
On September 6, 2019, at 1009 Pacific daylight time, a Piper PA-18, N14365, was substantially damaged when it was involved in an accident near Hood River, Oregon. The certificated flight instructor (CFI) and private pilot were fatally injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.
A witness observed the airplane during takeoff from Ken Jernstedt Airport (4S2), Hood River, Oregon. The witness stated it appeared as if it was in slow flight with a nose-high angle of attack. He observed the nose of the airplane pitch down, which he attributed to corrective action by the pilots, when the engine abruptly lost power. The witness reported the right wing started to drop and the airplane was half-way through a rotation/spin when it impacted the ground. He estimated that the airplane was no more than 100 ft above ground level (agl).
Another witness was in the grass area on the west side of the runway marshalling airplanes to parking spots for an annual fly-in. He observed the airplane taxi and takeoff, with the engine producing full power. As the airplane was climbing after takeoff, he heard the engine lose power abruptly. The witness observed the airplane’s nose lower “as if it was trying to gain airspeed,” while the airplane began a turn to the right. The nose continued to lower, and the rate of rotation increased until the witness lost site of the airplane behind the T-hangars.
The airplane came to rest on the northside of runway 25 adjacent to T-hangars, about mid-span of the T-hangar row, on a southerly heading facing the runway. The cockpit of the airplane came to rest upright.
First responders reported that the fuel selector valve was found in the OFF position when they arrived onsite. They also noted fuel leaking from the airplane.
A postaccident examination of the airplane revealed the fuselage/cockpit area sustained impact damage with aft crushing. The carburetor heat lever was out (ON position) and bent down. The mixture lever was in the full rich position. The primer pump was in and locked. The flaps were in the UP position and the throttle lever was positioned between OPEN and CLOSED. Flight control continuity was established from the cockpit to each flight control surface. The fuel selector was in place on the left cabin wall. The selector was in the OFF position and the pointer had been folded over toward the handle. The indicator plate displayed a red witness mark adjacent to the fuel selector pointer under one of the OFF-indicator marks. When the indicator plate was removed, some fuel was leaking from the fuel selector and fuel lines. Air was blown through each fuel inlet with no blockages noted. The selector position was moved from each detent position (OFF, LEFT, RIGHT) without obstruction.
The engine remained attached to the engine mounts and was pushed aft into the firewall. Manual rotation of the engine produced mechanical and valve-train continuity, with thumb compression obtained at all cylinders. Both magnetos remained attached to their respective mounting pads in their normal location on the engine. The magnetos were removed and produced spark at each of the leads when tested.
The top four spark plugs were removed; their electrodes exhibited normal wear. When the carburetor was opened, there was fuel in the bowl that was blue in color and smelled like avgas. There was about 1 inch of fuel in the bowl.
According to a representative of the airplane manufacturer, the aircraft’s basic empty weight was calculated to be 1,086.2 pounds (lbs.). The weight at the time of the accident was calculated to be 1,771.4 lbs. This calculation factored in the reported weight of the occupants (479 lbs. total), the fuel weight reported by the operator (full tanks less 20 minutes' flight time, 196.2 lbs.) as well as the 10 lbs. of miscellaneous items (oil bottles, documents, etc.) that appeared to be aboard. The Type Certificate Data Sheet for the airplane listed 1,750 lbs. as the Normal Category Max Weight for the PA-18-150.
A review of airport security video footage showed the airplane in a right descending turn before it impacted the ground.
Autopsies were performed on both occupants by the Oregon State Medical Examiner's Office. The cause of death for the CFI (seated in the rear seat) was listed as “blunt force head injury.” The cause of death for the private pilot (seated in the front seat) was listed as “multiple blunt force injuries.”
Toxicology testing was performed at the Federal Aviation Administration (FAA) Forensic Sciences Laboratory, for both occupants. The testing found no drugs of abuse for the private pilot.
The results from the CFI’s testing identified 14 (mg/dL) glucose in the vitreous and 6 (mg/dL) glucose in the urine. Quinine was also detected (but not quantified) in the CFI’s blood and urine. Quinine is a prescription medication used alone or with other medications to treat malaria in certain parts of the world. Quinine has also been used to control severe nighttime leg cramps (however, this use is not approved by the Food and Drug Administration). In addition, commercially available tonic water may also have small amounts of quinine. Adverse side effects have been noted depending on the concentration.
Data Source
Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# WPR19FA251