N1085W

Substantial
None

Mooney M20MS/N: 27-0043

Accident Details

Date
Saturday, September 14, 2019
NTSB Number
GAA19CA546
Location
Chandler, AZ
Event ID
20190914X20733
Coordinates
33.269721, -111.814163
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

The pilot's improper pitch control during takeoff and his exceedance of the airplane’s critical angle of attack, which resulted in an aerodynamic stall. Contributing to the accident was the flight instructor's failure to take remedial action.

Aircraft Information

Registration
Make
MOONEY
Serial Number
27-0043
Engine Type
Reciprocating
Year Built
1990
Model / ICAO
M20MM20P
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
4
FAA Model
M20M

Registered Owner (Current)

Name
BAS PART SALES LLC
Address
575 ED BEEGLES LN
City
GREELEY
State / Zip Code
CO 80631
Country
United States

Analysis

The pilot reported that, during a familiarization flight with a flight instructor in a recently purchased, retractable landing gear-equipped airplane, while demonstrating a soft field takeoff, the tower controller cleared him for takeoff "with no delay." He quickly taxied the airplane to the runway centerline, applied power, and pulled back on the yoke. He added that, in retrospect, the back pressure used was too abrupt. The airplane entered ground effect about 10 knots slower than normal and was unable to maintain flight in ground effect and he was struggling to maintain runway heading. The airplane touched down "abruptly several times." The airplane drifted to the left and he thought he had a positive rate of climb, so he retracted the landing gear. Additionally, he was "too aggressive" with control inputs and "caused a stall." The left wing struck the taxiway and the airplane came to rest on the ramp. The pilot reported that the instructor did not take the flight controls.

The flight instructor did not provide a statement to the NTSB.

The airplane sustained substantial damage to the left wing.

The pilot reported that there were no preaccident mechanical failures or malfunctions with the airplane that would have precluded normal operation.

The airport's automated weather observation station reported that, about 5 minutes after the accident, the wind was from 090° at 13 knots. The pilot was departing on runway 04L.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# GAA19CA546