HB-JCC

MINR
Unknown

AIRBUS BD-500-1A11 (CS300)S/N: 55012

Accident Details

Date
Tuesday, October 15, 2019
NTSB Number
ENG20LA001
Location
West Flanders Province, Belgium
Event ID
20191016X82836
Coordinates
50.993420, 2.795200
Aircraft Damage
MINR
Highest Injury
Unknown
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
0

Probable Cause and Findings

A No. 1 (left) engine low pressure compressor (LPC) stage 1 integrally bladed rotor (IBR) separation due to a high cycle fatigue crack (HCF) that originated at the runout of an airfoil leading edge root radius. The HCF crack developed because of a mechanically coupled LPC stage 3 and stage 1 IBR mode excitation and blade flutter response. The excitation was driven by an acoustic tone generated by turbulent airflow passing over the 2.5 bleed valve duct cavity while the engine was operating at high speeds in specific flight conditions. A primary contributor to the failure mode was an electronic engine control (EEC) software update that changed the LPC vane schedule and increased the likelihood of LPC stage 1 IBR blade flutter onset within the engine operating range.

Aircraft Information

Registration
HB-JCC
Make
AIRBUS
Serial Number
55012
Model / ICAO
BD-500-1A11 (CS300)

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ENG20LA001