N11379

Substantial
Minor

Cessna 206S/N: 20608077

Accident Details

Date
Friday, October 18, 2019
NTSB Number
WPR20LA009
Location
Stockton, CA
Event ID
20191017X22012
Coordinates
37.895557, -121.259445
Aircraft Damage
Substantial
Highest Injury
Minor
Fatalities
0
Serious Injuries
0
Minor Injuries
2
Uninjured
0
Total Aboard
2

Probable Cause and Findings

A total loss of engine power after takeoff for reasons that could not be determined based on the available information.

Aircraft Information

Registration
Make
CESSNA
Serial Number
20608077
Engine Type
Reciprocating
Year Built
1999
Model / ICAO
206C206
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
6
FAA Model
206H

Registered Owner (Current)

Name
BAS PART SALES LLC
Address
575 ED BEEGLES LN
City
GREELEY
State / Zip Code
CO 80631
Country
United States

Analysis

On October 17, 2019, about 1800 Pacific daylight time, a Cessna 206H airplane, N11379, was substantially damaged when it was involved in an accident near Stockton, California. The flight instructor and private pilot receiving instruction sustained minor injuries. The airplane was operated as a 14 Code of Federal Regulations Part 91 instructional flight.

The flight instructor reported that the purpose of the flight was to practice instrument approaches. After a thorough preflight and engine run-up, the pilot took off from runway 29L. About 150 feet above the ground, the engine “surged” then “smoothed out.” The airplane continued to climb, but the pilots elected to conduct a precautionary landing. The pilot continued the climb and made a left turn for the traffic pattern. During the turn, the engine lost total power at 380 feet above the ground and the instructor took control of the airplane. He landed the airplane in an empty lot; the airplane continued through a perimeter fence and impacted a semi-trailer parked along an adjacent roadway. The airplane came to rest nose down against the fence and semi-trailer. The left wing and forward fuselage sustained substantial damage.

Postaccident engine examination by the Federal Aviation Administration revealed no visual indications of catastrophic engine failure. The ignition leads were inspected and produced spark with normal impulse coupling operation. The spark plugs were removed and exhibited signatures consistent with a rich/low power condition. The rocker covers were removed. When the propeller was rotated, valve train continuity was established throughout, and thumb compression was established on all cylinders. The electric fuel pump was turned on and low fuel pressure was noted at fuel injectors to the cylinder heads. The fuel line between the fuel servo and the fuel distributor was removed and low fuel pressure was noted. The fuel pump was tested, and fuel pumped normally to the inlet of the fuel servo.

The fuel servo was removed from the engine for an operational test and teardown. After a visual examination, it was installed onto a test stand and operated slightly below manufacturer’s specifications. The fuel servo was removed from the test stand and the fuel screen was removed; no debris was present. Disassembly of the metering section did not reveal any anomalies that would have precluded normal operation. A Lycoming representative reported that, although the fuel flow was slightly below specifications, the engine still would have had adequate fuel to operate normally.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# WPR20LA009