N686DR

Substantial
None

Beech 55S/N: TC-1049

Accident Details

Date
Saturday, November 9, 2019
NTSB Number
ERA20LA035
Location
Griffin, GA
Event ID
20191109X14019
Coordinates
33.226943, -84.275001
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
6
Total Aboard
6

Probable Cause and Findings

The pilot’s failure to ensure that the airplane was properly configured for takeoff, which resulted in the inadvertent retraction of the landing gear during the takeoff roll and the airplane’s subsequent runway excursion.

Aircraft Information

Registration
N686DR
Make
BEECH
Serial Number
TC-1049
Engine Type
Reciprocating
Year Built
1967
Model / ICAO
Aircraft Type
Fixed Wing Multi Engine
No. of Engines
2

Registered Owner (Historical)

Name
LINDSEY CHARLES A
Address
433 S MAIN ST
Status
Deregistered
City
MADISON
State / Zip Code
GA 30650-1611
Country
United States

Analysis

On November 9, 2019, at 1024 eastern daylight time, a Beech BE55, N686DR, was substantially damaged when it was involved in an accident near Griffin, Georgia. The commercial pilot and four passengers were not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

The pilot reported that he was giving rides in his airplane, and the accident flight was the fifth flight of the morning. After the passengers boarded, the pilot taxied to runway 14 and completed the before takeoff checklist, then applied full power for takeoff. He reported that everything appeared normal during the takeoff roll, but, as the airplane approached 70 knots, about one third of the way down the runway, the landing gear suddenly retracted, and the airplane skidded off the right side of the runway before coming to rest partially on the grass and runway pavement.

Following the accident, the pilot noticed that the landing gear handle was in the up position; he reported that it may have been accidentally bumped by one of the passengers as they got into the airplane.

Examination of the airplane by a Federal Aviation Administration inspector revealed that the airplane sustained substantial damage to the underside of the fuselage. A subsequent follow-up examination of the airplane and landing gear system revealed that the gear handle operated normally, and the landing gear functioned as designed. No anomalies were discovered with the system that would preclude normal landing gear operation.

Maintenance was performed on the landing gear handle on January 19, 2018, at an airframe total time of 3,896 hours; the landing gear control handle was loose due to a selector handle spring retainer irregularity. The landing gear handle was repaired, and functionality was verified. There were no additional maintenance irregularities noted with the system during subsequent maintenance and the pilot reported no issues with the landing gear since the maintenance was performed 22 months before the accident.

The airplane’s "initial" checklist included a line item stating "gear lever – down." According to the airplane flight manual landing gear systems description, the airplane was equipped with a safety switch to prevent inadvertent retraction of the landing gear on the ground; a main strut safety switch opens the control circuit when the strut is compressed. A caution note stated, “Never rely on the safety switch to keep the gear down during taxi or on takeoff, landing roll, or in a static position. Always make certain that the landing gear switch is in the down position during these operations.”

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA20LA035