N5573M

Substantial
None

Aero Commander 100S/N: 107

Accident Details

Date
Saturday, January 4, 2020
NTSB Number
CEN20LA055
Location
Mullin, TX
Event ID
20200104X82940
Coordinates
31.650278, -98.654167
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

A total loss of engine power for reasons that could not be determined based on the available information.

Aircraft Information

Registration
N5573M
Make
AERO COMMANDER
Serial Number
107
Engine Type
Reciprocating
Year Built
1967
Model / ICAO
100VO10
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
CLAY JEREMY N
Address
582 PRIVATE ROAD 1387
Status
Deregistered
City
DUBLIN
State / Zip Code
TX 76446-4523
Country
United States

Analysis

On January 4, 2020, about 1600 central standard time, an Aero Commander 100 airplane, N5573M, sustained substantial damage when it was involved in an accident near Mullin, Texas. The student pilot and flight instructor were not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 instructional flight.

The flight instructor reported that he and the student departed on the 75-nautical-mile flight with 40 gallons of fuel onboard. About 3 miles from the destination airstrip, they initiated a slow descent to a private airstrip. The student completed the Descent and the Before Landing checklist. About 3,000 ft above mean sea level, the engine lost total power.

The instructor immediately took control of the airplane and ensured that the fuel selector switch was selected for both fuel tanks, the carburetor heat was applied, and the mixture control was at the full-rich position. He trimmed the airplane for its best glide speed and the student completed a mayday call. The instructor switched fuel tanks; however, the engine did not respond, and the propeller was “wind milling.” The instructor performed a forced landing to a flat, plowed dirt field, during which the right wingtip impacted a tree and the airplane nosed over.

The airplane sustained substantial damage to the fuselage, both wings, and the empennage. The fuel system was breached during the accident and the exact amount of fuel onboard at the time of the loss of engine power could not be determined. The airplane was recovered from the accident site and an engine run was performed. The engine successfully ran for several minutes at various power settings when a fuel source was plumbed to the engine. No mechanical anomalies were found during the engine run.

Examination of the fuel selector revealed that either the fuel selector handle or the pointer was installed 180° out of position. When the selector handle was selected to BOTH, the valve was completely closed, in what should have been the OFF position. When the selector handle was selected to OFF, the valve was open, in what should have been the BOTH position. The hole on the end of the pointer that slid over the shaft featured a round side and a flat side, which helps to correctly orient the pointer during installation. The hole was sufficiently worn that the pointer would fit over the shaft in both directions. The examination could not determine if the selector handle or the pointer was installed incorrectly.

The temperature and dewpoint for the accident time and accident site were not conducive to the formation of carburetor icing.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# CEN20LA055