N420PW

Destroyed
Fatal

Vans VANS RV-6S/N: 20181

Accident Details

Date
Sunday, January 5, 2020
NTSB Number
ERA20FA063
Location
Cullman, AL
Event ID
20200105X53312
Coordinates
34.272777, -86.858055
Aircraft Damage
Destroyed
Highest Injury
Fatal
Fatalities
2
Serious Injuries
0
Minor Injuries
0
Uninjured
0
Total Aboard
2

Probable Cause and Findings

The pilot’s inadequate planning, which resulted in fuel exhaustion and a total loss of engine power during the initial climb. Also causal was the pilot’s exceedance of the airplane’s critical angle of attack while attempting to return to the runway after takeoff, which resulted in an aerodynamic stall/spin, loss of control, and impact with terrain.

Aircraft Information

Registration
N420PW
Make
VANS
Serial Number
20181
Model / ICAO
VANS RV-6

Registered Owner (Historical)

Name
MACKENTEPE JOSEPH P
Address
21391 US HIGHWAY 31
Status
Deregistered
City
VINEMONT
State / Zip Code
AL 35179-5989
Country
United States

Analysis

On January 5, 2020, about 1243 central standard time, an experimental, amateur-built Vans RV-6, N420PW, was destroyed when it was involved in an accident near Cullman, Alabama. The private pilot and passenger were fatally injured. The airplane was operated as a Title 14 Code of Federal Regulations (CFR) Part 91 personal flight.

A review of airport surveillance video revealed that the pilot and passenger arrived about 1230. At 1240, the airplane was seen on the taxiway, where it stopped for a moment before continuing to the active runway. At 1242, the airplane was seen climbing from runway 02, when the video stopped recording.

According to witnesses, the airplane taxied to runway 02 and began the takeoff roll. During the initial climb, when the airplane reached about 350 ft above the ground, a loud “pop” was heard. The witnesses watched as the airplane entered an immediate “sharp left banking turn” in what appeared to be an attempt to return to the airport. The airplane “stalled and went into a left spiral downward turn.” The airplane completed two turns before colliding with the ground on airport property adjacent the taxiway. Several other witness described a similar series of events, including the engine making a “pop” noise and/or a loss of engine power prior to the airplane making a steep turn back toward the runway before descending to the ground. The airport authorities and witnesses responded immediately to the accident scene.

AIRPLANE INFORMATION

Review of the airplane’s maintenance records revealed that it’s most recent condition inspection was completed in 2014.

The airplane’s co-owner stated that the pilot had flow the airplane from Cullman Regional Airport (CMD), Cullman, Alabama to Auburn University Regional Airport (AUO), Auburn, Alabama around December 31, 2019. During the return flight from AUO to CMD, the pilot had diverted to Hartselle/Morgan County Regional Airport (5M0), Hartselle, Alabama due to the wind conditions at CMD. The estimated total distance for the trip was about 260 nautical miles. The co-owner did not know when the airplane had been brought back to CMD, nor whether it had flown between then and the accident flight. Review of fueling records at CMD revealed that the airplane was last fueled on November 29, 2019, with 18.7 gallons of 100LL aviation fuel.

WRECKAGE INFORMATION

The airplane impacted terrain about 1,500 ft from the departure end of runway 02. All flight control surfaces were located at the accident site. The cockpit was crushed to the bulkhead of the fuselage. The instrument panel was crushed and the instruments were impact-damaged. The instruments did not display any reliable information due to impact damage.

There was no post-crash fire, and although the fuel tanks were breached, there was no residual fuel noted onsite. Examination of the fuel selector revealed that the selector was between the left and right fuel tank. Pressurized air was supplied to the fuel selector, and it was discovered that when positioned between both tanks, fuel was only supplied from the left tank. The fuel selector was placed in the right tank position and pressurized air was supplied through the lines and the air moved to the right fuel tank line as noted on the selector. The selector was placed in the left fuel tank position and pressurized air was supplied through the lines and the air moved to the left fuel tank line as noted on the selector.

Examination of the engine revealed that the crankcase remained intact and displayed impact damage. There were no fractures in the case that would indicate a catastrophic internal engine failure. During the examination of the carburetor, the upper section was removed from the float bowl and was observed to be about ½ full of blue liquid with an odor consistent with aviation gasoline. A test of the liquid with water finding paste revealed no indication of water in the liquid. No damage was noted to the brass fuel floats or the needle and seat assembly. The engine-driven fuel pump remained attached to the engine and no damage was noted. The pump was removed and produced air from the outlet port when actuated by hand. Liquid with an odor consistent with aviation gasoline drained from the pump when it was removed and tilted. The pump was partially disassembled, and no damage noted to the internal check valves or the rubber diaphragms. No liquid drained from the fluid line from the airframe to the engine driven fuel pump or the fluid line from the pump to the carburetor when they were removed.

The cylinders were examined using a lighted borescope. The piston faces, cylinder bores, and valve heads displayed normal operating and combustion signatures. While rotating the vacuum drive it was noted that all four cylinders displayed thumb compression and suction. During rotation it was noted that all the rocker arms and valves moved accordingly. Examination of the magnetos revealed the left magneto was broken away from the accessory case and the right magneto remained attached. Both magnetos were rotated and both produced spark on all terminals. Examination of the propeller assembly revealed the two blade, constant speed propeller remained separated from the propeller flange and displayed impact damage signatures. Both propeller blades revealed “S” type bending and exhibited chordwise scratching. One blade displayed aft bending and twisting deformation.

MEDICAL AND PATHOLOGICAL INFORMATION

According to the autopsy performed by the University of Alabama’s Department of Pathology, the determined cause of death was multiple blunt force trauma and the manner of death was accident. No significant natural disease was identified.

Toxicology testing performed by the Alabama Department of Forensic Sciences identified benzoylecgonine in cavity blood.

Toxicology testing performed by the FAA’s Forensic Sciences Laboratory identified cocaine in urine but not in blood; its inactive metabolites, benzoylecgonine and ecgonine methyl ester, were identified in blood and urine. While no delta-9-tetrahydrocannabinol (THC, the psychoactive component in cannabis) was found in blood or urine, its active metabolite, 11-hydroxy-delta-9-THC, was found only in urine at 2.6ng/ml and its inactive metabolite, carboxy-delta-9-THC, was found in blood at 1.5 ng/ml and in urine at 15.2 ng/ml.

Cocaine is a central nervous system stimulant available for topical use by prescription as a Schedule II controlled substance; it has a high potential for abuse. THC is the primary psychoactive compound in cannabis and causes a variety of psychoactive symptoms.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA20FA063