N1612F

Destroyed
Fatal

Cessna 172S/N: 17255007

Accident Details

Date
Monday, January 6, 2020
NTSB Number
ERA20FA068
Location
Newborn, GA
Event ID
20200106X65620
Coordinates
33.494445, -83.642501
Aircraft Damage
Destroyed
Highest Injury
Fatal
Fatalities
1
Serious Injuries
0
Minor Injuries
0
Uninjured
0
Total Aboard
1

Probable Cause and Findings

The pilot’s impairment/incapacitation from carbon monoxide poisoning due to a degraded muffler. Contributing to the accident was the pilot’s failure to properly maintain the airplane.

Aircraft Information

Registration
N1612F
Make
CESSNA
Serial Number
17255007
Engine Type
Reciprocating
Year Built
1966
Model / ICAO
172C172
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
DEKLE MILLWOOD ASHLEY
Address
295 SWIFT ST
Status
Deregistered
City
TOCCOA
State / Zip Code
GA 30577-5937
Country
United States

Analysis

HISTORY OF FLIGHTOn January 6, 2020, at 1423 eastern standard time, a Cessna 172H, N1612F, was destroyed when it was involved in an accident near Newborn, Georgia. The pilot was fatally injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

The pilot, who owned the airplane, departed Toccoa Airport-RG Letourneau Field (TOC), Toccoa, Georgia, about 1230 and was destined for Cairo-Grady County Airport (70J), Cairo, Georgia, about 240 nautical miles away. The pilot’s daughter stated that he was likely flying to Cairo to look for property in the area.

Radar track data provided by the Federal Aviation Administration (FAA) showed a target correlated to be the accident airplane after departure from TOC. The airplane proceeded on a heading of about 170° for 15 miles, taking a right turn to about 233° for 5 miles, then turning south again to 190° for an additional 25 miles. About 1 hour into the flight, the airplane turned west-southwest (figure 1) in a meandering track for about 10 miles in the vicinity of Newborn; it then made a right turn to the north and completed several left 360° turns before turning back to the east and completing two additional right 360° turns. The airplane proceeded to the north briefly, completing several 360° turns before continuing into 13 360° right turns that progressed in an easterly direction until radar contact was lost near the accident site (figure 2). The pilot’s daughter stated that she thought there was no reason why the pilot would be looking at property in Newborn from the air.

Two witnesses observed the airplane flying low just before the accident, and another witness stated that the airplane was circling and then descended below the tree line. The airplane impacted terrain, and a postaccident fire ensued.

Figure 1 - Overview of final route of flight.

Figure 2 - Final flight track through loss of radar near accident site.

PERSONNEL INFORMATIONAccording to FAA airmen records, the pilot, age 72, held a private pilot certificate with a rating for airplane single-engine land. The pilot reported 344 hours total flight time as of his most recent aviation medical exam on November 15, 2013. The pilot’s last entry in his logbook was on July 16, 2019; his total flight time was 358.65, of which 1/4 hour was during the previous 6 months.

AIRCRAFT INFORMATIONThe airplane’s most-recent annual inspection was completed on September 17, 2018. Only three other records of maintenance were found for the 10 years before the accident: two annual inspections on May 27, 2013, and November 18, 2010, and replacement of the left muffler on April 1, 2010. There was no documentation in the records that showed installation of, or maintenance performed to, the right muffler. The airplane had been operated about 93 hours over that period. The mechanic who conducted the 2013 annual inspection and almost all of the airplane’s maintenance from 2008 to 2013 knew the airplane well and considered the pilot a friend; he stated that the airplane was in “rough shape.” Within the last few years, the pilot had asked him to conduct maintenance on the airplane; there were issues with the electrical system and a flap. The mechanic stated he didn’t want to “touch” the airplane unless the pilot agreed to a comprehensive annual inspection. The pilot declined and elected to take it to another mechanic.

AIRPORT INFORMATIONThe airplane’s most-recent annual inspection was completed on September 17, 2018. Only three other records of maintenance were found for the 10 years before the accident: two annual inspections on May 27, 2013, and November 18, 2010, and replacement of the left muffler on April 1, 2010. There was no documentation in the records that showed installation of, or maintenance performed to, the right muffler. The airplane had been operated about 93 hours over that period. The mechanic who conducted the 2013 annual inspection and almost all of the airplane’s maintenance from 2008 to 2013 knew the airplane well and considered the pilot a friend; he stated that the airplane was in “rough shape.” Within the last few years, the pilot had asked him to conduct maintenance on the airplane; there were issues with the electrical system and a flap. The mechanic stated he didn’t want to “touch” the airplane unless the pilot agreed to a comprehensive annual inspection. The pilot declined and elected to take it to another mechanic.

WRECKAGE AND IMPACT INFORMATIONThe airplane impacted dense woods and terrain about 3 miles east of Newborn, Georgia. The wreckage path was on a magnetic heading of about 215° and was about 180 ft long. The airplane came to rest inverted. Both wings separated during impact, and the fuselage was consumed by a postimpact fire. All airframe, control surfaces, and engine components were located at the scene, and several smaller pieces of aluminum, plexiglass, wheel fairing, and a door were found along the wreckage path among broken tree limbs and branches. The propeller was found in the engine impact crater and was sheared off the hub during the impact; it exhibited gradual aft bending and had a few diagonal chordwise scrapes on the blades.

Flight control cable continuity was confirmed through multiple overload breaks and failures. The left- and right-wing fuel tanks were ruptured and thermally damaged. The left fuel cap was secured in place, and the right fuel cap was melted but remained attached to the chain that was secured in place.

The left and right flaps and associated actuators were found in the up (stowed) position.

The engine remained largely intact, although there was significant thermal damage on the aft section of the engine near the firewall. The spark plugs were removed and examined. They appeared to have minimal wear when compared to the Champion Check-A-Plug chart and did not display any evidence of carbon or lead fouling that would preclude normal operation. Engine thumb compression and suction on all cylinders were confirmed, and crankshaft continuity was confirmed from the front to the accessory gear section of the engine through a full 720° of rotation. The engine examination did not reveal any preimpact anomalies that would preclude normal operation.

The left and right mufflers, and their respective shrouds, had separated during the accident sequence and were found partially buried in mud, protected from the postaccident fire. They were sent to the National Transportation Safety Board (NTSB) Materials Laboratory for a detailed examination.

The left smooth muffler exterior surface was sound with no evidence of cracks or through-thickness metal wastage. The right muffler and shroud exhibited substantial mechanical damage. The aft face of the muffler with inlet tube was separated from the assembly and was not recovered. The right smooth muffler surface exhibited cracks and through-thickness metal wastage. The fractures associated with the separation of the aft face with inlet tube exhibited largely oxidized fracture surfaces and thinned walls. The center inlet tube was separated from the rest of the muffler due to loss of mechanical integrity from metal wastage. Holes and wall thickness loss were also noted around the muffler body.

A metallurgical cross-section taken through an exemplar area of metal wastage showed evidence of general thermal oxidative loss of material wall thickness as well as through-thickness holes and cracks. There were metal wastage and wall-thickness though-holes adjacent to the crimp seal between the muffler tube and the forward end plate as well.

Due to the extensive postaccident fire damage to the fuselage, the NTSB was unable to determine if the airplane was equipped with any type of carbon monoxide detection equipment.

MEDICAL AND PATHOLOGICAL INFORMATIONAccording to the autopsy performed by the Division of Forensic Sciences, Georgia Bureau of Investigation, the cause of death was multiple blunt force injuries and carbon monoxide toxicity. In addition, moderate atherosclerotic stenosis (70%) of the left anterior descending coronary artery and mild atherosclerotic stenosis (30%) of right coronary artery were identified.

Toxicology testing performed by the Division of Forensic Sciences, Georgia Bureau of Investigation, identified 61% carboxyhemoglobin in cavity blood. Additional toxicology testing performed by the FAA’s Forensic Science Laboratory identified 48% carboxyhemoglobin in cavity blood as well as bupropion (a potentially sedating antidepressant) and one of its metabolites, citalopram (generally considered a nonsedating antidepressant) and one of its metabolites, trace amount of diphenhydramine (a sedating antihistamine), diltiazem (a blood pressure medication), atorvastatin (a cholesterol-lowering drug), sildenafil (used to treat erectile dysfunction) and one of its metabolites, and a metabolite of aspirin in the pilot’s blood and/or tissues.

Medical Records

Personal medical records were obtained from the pilot’s primary care doctor. These records were limited to a single visit to obtain bloodwork before a cardiac catherization; they did not contain a medical history or list of medications. The bloodwork was unrevealing. A copy of the cardiology record was included.

The cardiology record from a visit dated October 21, 2019, documented that the pilot had known coronary artery disease, paroxysmal atrial fibrillation, a previous stroke, high blood pressure, arthritis, and carotid artery disease. At the time, his daily medications included diltiazem, lisinopril (another blood pressure medication), omeprazole, atorvastatin, sildenafil, citalopram, lorazepam (a sedating benzodiazepine), and Eliquis (a blood thinner). He had undergone a cardiac catheterization on July 25, 2019, which demonstrated severe calcific diffuse coronary artery disease that was not amenable to procedural intervention.

At the time of the pilot’s last FAA medical examination in 2013, he had reported having high blood pre...

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA20FA068