N3672K

Destroyed
Fatal

Piper PA28S/N: 28-23682

Accident Details

Date
Friday, January 24, 2020
NTSB Number
WPR20FA079
Location
Payson, AZ
Event ID
20200124X92932
Coordinates
34.158889, -111.493888
Aircraft Damage
Destroyed
Highest Injury
Fatal
Fatalities
1
Serious Injuries
2
Minor Injuries
0
Uninjured
0
Total Aboard
3

Probable Cause and Findings

The pilot's decision to fly into a canyon with rising terrain, and his subsequent loss of aircraft control while maneuvering away from rising terrain.

Aircraft Information

Registration
Make
PIPER
Serial Number
28-23682
Engine Type
Reciprocating
Year Built
1967
Model / ICAO
PA28P28A
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1
Seats
4
FAA Model
PA-28-140

Registered Owner (Current)

Name
EGBERT COLTON T
Address
655 COUNTRY DR
City
FERNLEY
State / Zip Code
NV 89408-9018
Country
United States

Analysis

HISTORY OF FLIGHTOn January 24, 2020, about 0911 mountain standard time, a Piper PA28-140, airplane, N3672K, was destroyed when it was involved in an accident near Payson, Arizona. One of the two passengers was fatally injured, and the pilot and other passenger were seriously injured. The airplane was operated by the pilot as a Title 14 Code of Federal Regulations Part 91 personal flight.

The pilot stated in an interview that after a flight earlier that morning from Falcon Field Airport (FFZ), Mesa, Arizona, he landed in PAN, refueled, and departed for the return flight back to FFZ. During the return flight, the pilot decided to fly over the mountains southwest of their position. He stated that he flew about 1,000 ft above ground level (agl) over the mountains, while the passengers were spotting wildlife on the terrain below. The pilot stated the airplane was running well and that he didn’t remember anything else about the flight until 5 hours later, when he woke up injured, laying in a small creek at the accident site.

Radar flight track data showed the airplane depart PAN and fly to the Mazatzal Mountain Range. While maintaining an altitude of about 1,000 ft agl above the mountainous terrain, the airplane made a 280° turning maneuver, then descended over and into a canyon with rising terrain. (see Figure 1). About a half mile from the accident site, the flight track showed the airplane turn left and the turn radius increased before the track data stopped. The airplane’s groundspeed through the canyon decreased from 88 to 65 knots and the airplane’s altitude above the ground decreased from about 1,000 ft to 330 ft agl near the accident site. The terrain elevation rose about 800 ft up the canyon. The last recorded flight track data point was located about 500 ft from the accident site.

Figure 1-Flight track data and accident site location

WRECKAGE AND IMPACT INFORMATIONExamination of the accident site revealed the airplane was destroyed by impact forces, on steep, heavy brush covered terrain. The wreckage, including all major structural airplane components and primary flight controls, were contained within the debris path that was about 145 ft long and oriented on a magnetic heading of about 35°, paralleling and uphill from a small stream. (see Figure 2)

Figure 2-Accident site aerial view.

The outboard right-wing sections revealed leading-edge circular impact damage, similar in size to the large trees near the beginning of the debris path. The circular impact damage was found on the lower forward side of the wing near the leading edge, consistent with the airplane positioned in a nose up attitude at the time of impact with the ground.

The propeller was found about halfway through the debris field and the blades revealed leading edge gouging and loss of blade material at the tips. The main wreckage, including the engine were found on top of the rocks located along the stream. The cabin and forward fuselage were mostly consumed by postimpact fire. The left wing and empennage were found partially attached to the main wreckage and had postimpact fire damage.

The wreckage was recovered to a secure facility for further examination. Flight control cable continuity was attained through multiple overload fractures. The exhaust muff was disassembled and examined, and no anomalies were noted. The examination revealed no anomalies with the airframe or engine that would have precluded normal operation.

MEDICAL AND PATHOLOGICAL INFORMATIONThe Gila County Regional Medical Examiner’s Office, Reno Nevada, performed an autopsy on the passenger. The cause of death was noted as multiple blunt force trauma.

Toxicology testing on the passenger’s specimens indicated carbon monoxide levels less than 10% saturation.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# WPR20FA079