N982SS

Substantial
None

AugustaWestland AW119MKIIS/N: 14962

Accident Details

Date
Saturday, March 21, 2020
NTSB Number
ERA20CA135
Location
Philadelphia, PA
Event ID
20200322X70803
Coordinates
40.083332, -75.001388
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

The in-flight failure of the lower left side of the engine cowling due to the mechanic’s improper installation of the fasteners, which resulted in the cowling impacting all four main rotor blades.

Aircraft Information

Registration
N982SS
Make
AUGUSTAWESTLAND
Serial Number
14962
Year Built
2020
Model / ICAO
AW119MKII

Registered Owner (Historical)

Name
AGUSTAWESTLAND PHILADELPHIA CORP
Address
3050 RED LION RD
Status
Deregistered
City
PHILADELPHIA
State / Zip Code
PA 19114-1128
Country
United States

Analysis

The pilot and the flight test engineer had just completed a production test flight of the helicopter and were preparing to land when the lower section of the left side of the engine cowling folded back and struck all 4 main rotor blades and made contact with all 4 main rotor blades at some point prior to the rotor stopping, resulting in substantial damage. According to the operator/manufacturer, none of the fasteners on the left side of the cowling remained attached and 3 of the fasteners were missing.Prior to the flight, the pilot observed that the fasteners attaching the generator duct to the right side of the same cowling appeared long and reported it to maintenance. No anomalies were observed with the fasteners attaching the cowling tothe airframe. Maintenance then removed the one-piece engine cowling and a mechanic replaced the generator duct fasteners before reinstalling the cowling with the help of another mechanic. The mechanic said he specifically fastened each of the fasteners on the cowling himself and did a 100% check of each fastener after the cowling was installed. Once the cowling was reinstalled a quality inspector visually inspected the engine cowling fasteners. He did not observe any anomalies and signed off that the work had been completed. Prior to the accident flight, the flight test engineer performed another preflight inspection of the helicopter and did not observe any obvious issues with any of the cowling fasteners. The helicopter then departed and flew for about an hour before the cowling folded back. Postaccident examination of the cowling by the operator/manufacturer revealed no evidence of any preaccident discrepancies with the fasteners/cowling, or the design and conformity of the helicopter structure.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# ERA20CA135