N7997N

Substantial
None

TL Ultralight SRO StingsportS/N: TLUSA136

Accident Details

Date
Saturday, March 28, 2020
NTSB Number
WPR20LA116
Location
Hurricane, UT
Event ID
20200331X23804
Coordinates
37.140277, -113.306110
Aircraft Damage
Substantial
Highest Injury
None
Fatalities
0
Serious Injuries
0
Minor Injuries
0
Uninjured
2
Total Aboard
2

Probable Cause and Findings

A total loss of engine power due to the failure of the ignition system as a result of foreign object damage.

Aircraft Information

Registration
N7997N
Make
TL ULTRALIGHT SRO
Serial Number
TLUSA136
Engine Type
Reciprocating
Year Built
2006
Model / ICAO
StingsportAC4
Aircraft Type
Fixed Wing Single Engine
No. of Engines
1

Registered Owner (Historical)

Name
CUTTS RICHARD E
Address
1222 N SUNSET RIDGE DR
Status
Deregistered
City
HURRICANE
State / Zip Code
UT 84737-2556
Country
United States

Analysis

On March 28, 2020, about 1447 mountain daylight time, a TL Ultralight SRO Stingsport airplane, N7997N, was substantially damaged when it was involved in an accident at the General Dick Stout Field Airport (1L8), Hurricane, Utah. The commercial pilot and passenger were not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91, personal flight.

According to the pilot, shortly after takeoff and about 250 ft above ground level, the engine abruptly lost power. The pilot attempted to land on the remaining runway but was unable and touched down in a field. During the landing sequence, the airplane bounced, which resulted in the collapse of the landing gear and the airplane skidding to a stop.

Examination of the engine by a Federal Aviation Administration-certified mechanic revealed no anomalies with the engine except for the ignition system. The ignition system was observed to have damage to the stator assembly. The ignition system was removed and sent to the engine manufacturer for examination. The ignition consisted of a stator assembly, magneto ring, flywheel hub, and associated electronic modules and coils. Examination of the stator assembly revealed that the component had sustained damage to the only two independent ignition charging coils that were attached to the assembly. The damage on the ignition charging coils was consistent with foreign object damage. The ignition charging coils were tested and failed and were determined to be nonfunctional. The failure of both ignition charging coils would result in the loss of engine power.

Additional examination of the magneto ring revealed gouges and scoring marks that were consistent with foreign object damage. The ignition charging coils were positioned below the area where the scoring and gouges of the magneto ring were observed. No remnants of the foreign object damage remained, and its source was unable to be determined. All the other ignition components were examined and tested, and no anomalies were noted.

Data Source

Data provided by the National Transportation Safety Board (NTSB). For more information on this event, visit the NTSB Records Search website. NTSB# WPR20LA116